Mechanical & Engine Failure · NTSB ANC14FA050

PIPER PA 12 — Anchorage, AK

1 fatal
DateJuly 2, 2014
LocationAnchorage, AK
AircraftPIPER PA 12
Purpose of flightPersonal
ConditionsDay · Visual Meteorological Cond
Phase / occurrencePrior to flight Aircraft maintenance event
Pilot age61
Pilot total time400 hrs · Building experience
Time in typeUnknown
Fatalities1

Probable cause

The incorrect (reverse) rigging of the elevator control cables, and the pilot’s inadequate preflight inspection, which failed to detect the misrigging.

NTSB findings

  • Aircraft-Aircraft systems-Flight control system-Elevator control system-Incorrect service/maintenance - C
  • Personnel issues-Task performance-Inspection-Preflight inspection-Pilot - C
  • Personnel issues-Task performance-Maintenance-Installation-Other/unknown - C

What happened

The accident flight was the airplane's first flight after undergoing maintenance and modification over the course of several years. A witness reported that, during the takeoff, the airplane climbed steeply in an extreme, nose-high attitude until it "pivoted" at the apex of the climb and then entered a descent straight to the ground. The airplane's described motions are consistent with the airplane exceeding its critical angle of attack and entering an aerodynamic stall; crush damage to the nose of the airplane and the leading edges of the wings was consistent with a nearly vertical flight path at the time of impact. Examination of the wreckage revealed that the airplane's elevator control cables were misrigged, such that they were attached to the incorrect (opposite) locations on the upper and lower elevator control horn, resulting in a reversal of elevator control inputs. Maintenance logs for the airplane contained no entries more recent than 2007. Several people reported that the pilot often performed maintenance on the airplane; however, none indicated knowledge of who performed maintenance on the elevator controls. A "BEFORE TAKEOFF" checklist for the airplane included the item, "CONTROLS – FREE AND CORRECT." If the pilot had checked the elevator for correct motion before takeoff, he likely would have discovered that it was misrigged.

An editorial "what led to it / how to avoid it" analysis for this accident is generated separately and will appear here.

View the official NTSB docket →