Mechanical & Engine Failure · NTSB CEN10FA180

BEECH B36TC — Dayton, OH

2 fatal Low-time pilot
DateApril 1, 2010
LocationDayton, OH
AircraftBEECH B36TC
Purpose of flightPersonal
ConditionsDay · Visual Meteorological Cond
Phase / occurrenceEmergency descent Off-field or emergency landing
Pilot age50
Pilot total time182 hrs · Low time
Time in type93 hrs
Fatalities2

Probable cause

The complete loss of engine power due to failure of the No. 1 main bearing, and the secondary failure of a crankcase through-bolt and the fuel pump drive coupling. Contributing to the accident was the pilot's decision to attempt a return to the airport for a downwind forced landing, despite having an interstate highway and an open grass area short of the runway as available emergency landing sites.

NTSB findings

  • Aircraft-Aircraft power plant-Engine (reciprocating)-Recip eng rear section-Failure - C
  • Personnel issues-Action/decision-Info processing/decision-Decision making/judgment-Pilot - F

What happened

Approximately 1 minute after takeoff, as the airplane was about 1 mile southwest of the airport, the pilot reported an engine failure to air traffic controllers and initiated a return to the airport. One witness, located about 1 mile west of the airport, reported that the sound of the engine changed abruptly; noting that the engine seemed to lose power completely. Another witness, located near the airport, observed the airplane approach from the west and turn to align with the downwind runway. During the turn, the left wingtip struck the ground and the airplane impacted short of the runway. A postimpact fire ensued. Although the pilot initiated a return to the airport, an interstate highway and an open grass area short of the runway were both potentially available for an emergency landing. A postaccident examination of the engine revealed that the No. 1 (aft) main crankshaft bearing failed due to unknown circumstances. The progressive failure of the bearing likely precipitated secondary failures of the crankcase through-bolt and the fuel pump coupling, which resulted in a complete loss of engine power.

An editorial "what led to it / how to avoid it" analysis for this accident is generated separately and will appear here.

View the official NTSB docket →