VFR into IMC · NTSB CEN11FA133

PIPER PA-46-310P — Milaca, MN

2 fatal High-time pilotIMC
DateDecember 30, 2010
LocationMilaca, MN
AircraftPIPER PA-46-310P
Purpose of flightPersonal
ConditionsDay · Instrument Meteorological Cond
Phase / occurrenceEnroute-climb to cruise Loss of control in flight
Pilot age65
Pilot total time2,078 hrs · Experienced
Time in typeUnknown
Fatalities2

Probable cause

The pilot did not recover from an unusual attitude while operating in instrument meteorological conditions following a disconnect of the autopilot system for undetermined reasons. Contributing to the accident were the pilot’s lack of recent flight experience and impairment due to diphenhydramine.

NTSB findings

  • Personnel issues-Task performance-Use of equip/info-Aircraft control-Pilot - C
  • Environmental issues-Conditions/weather/phenomena-Turbulence-(general)-Not specified
  • Environmental issues-Conditions/weather/phenomena-Temp/humidity/pressure-Conducive to structural icing-Not specified
  • Personnel issues-Experience/knowledge-Experience/qualifications-Recent experience-Pilot - F
  • Aircraft-Aircraft systems-Auto flight system-Autopilot system-Not specified
  • Aircraft-Aircraft oper/perf/capability-Performance/control parameters-(general)-Not attained/maintained - C
  • Personnel issues-Physical-Impairment/incapacitation-OTC medication-Pilot - F
  • Environmental issues-Conditions/weather/phenomena-Ceiling/visibility/precip-Clouds-Effect on operation

What happened

About 20 minutes after departing on a cross-country flight, the pilot acknowledged the air traffic controller’s clearance to climb to 17,000 feet mean sea level (msl). Radar data indicated that the airplane reached a maximum altitude of 16,800 feet msl. The airplane then entered a right descending turn followed by a left descending turn. While in the left turn, the pilot informed the controller, “I lost my autopilot; I’m in an unusual attitude.” The pilot stated this same information two more times in response to transmissions by the controller. The pilot’s last transmission was that he was busy trying to recover the airplane. Witnesses heard the airplane flying overhead for several minutes, but they could not see it due to the low ceiling.

A postaccident examination of the airplane did not reveal any preaccident mechanical malfunctions or failures with the engine that would have precluded normal operation. Examination of the autopilot system revealed a loose screw inside the pitch servo housing. The screw was one of two that secured the high wattage resistor to the solenoid housing. Observed corrosion within the screw threads was consistent with the threads not being engaged in a nut or other internally threaded feature. No mechanical damage or arcing was visible on the screw. The operational impact of the loose screw is unknown.

The pilot’s instrument flying proficiency could not be determined. According to log records, the pilot last flew 4.5 months before the accident. The airplane was in instrument meteorological conditions when the pilot stated that he was trying to recover from the unusual attitude. The pilot did not follow prescribed procedures for an autopilot malfunction. Weather data indicates that the airplane most likely encountered turbulence and icing conditions during the flight; however, the airplane was equipped with an ice protection system. Although ethanol was found during the toxicology tests, the levels varied greatly among the tissue/fluid samples. The investigation was unable to determine if the presence of ethanol was from ingestion or from postmortem production or contamination. The detected level of diphenhydramine, an over-the-counter sedating antihistamine used to treat allergies, was above therapeutic levels and likely contributed to the pilot’s inability to recover from the unusual attitude.

An editorial "what led to it / how to avoid it" analysis for this accident is generated separately and will appear here.

View the official NTSB docket →