Fuel Exhaustion & Starvation · NTSB CEN11FA508
BEECH A36 — Williston, ND
| Date | July 26, 2011 |
| Location | Williston, ND |
| Aircraft | BEECH A36 |
| Purpose of flight | Personal |
| Conditions | Day · Visual Meteorological Cond |
| Phase / occurrence | Maneuvering-low-alt flying Fuel starvation |
| Pilot age | 53 |
| Pilot total time | 1,721 hrs · Experienced |
| Time in type | 1,596 hrs |
| Fatalities | 1, 1 serious |
Probable cause
NTSB findings
- Aircraft-Fluids/misc hardware-Fluids-Fuel-Fluid management - C
- Aircraft-Aircraft power plant-Engine fuel and control-Fuel distribution-Incorrect use/operation - C
- Personnel issues-Task performance-Use of equip/info-Use of equip/system-Pilot - C
What happened
The passenger reported that the purpose of the local flight was to take low-altitude aerial photographs of nearby ground structures and that, shortly before the accident, the pilot remarked that the engine was not operating normally and asked him to look for a suitable landing area. He believed that the engine was still running at that time. The pilot located an open landing area and was in the process of landing when the right wing collided with terrain. During the postaccident examination, about 18 gallons of usable fuel was recovered from the left wing fuel tank, and no usable fuel was recovered from the right wing fuel tank. The observed damage to the propeller blades was indicative of the engine producing at least idle power at the time of the accident. A postaccident examination of the airplane revealed no evidence of mechanical malfunctions or failures that would have precluded normal operation. Additionally, the engine demonstrated the ability to produce rated horsepower during an operational test run. A review of fueling records and recorded engine data from previous flights established that the partial loss of engine power was likely due to fuel starvation and not from a mechanical malfunction of the engine. Although the fuel selector was found positioned to draw fuel from the left wing fuel tank, it is likely that the pilot repositioned the selector from the right wing fuel tank when he detected the engine problem. Because he was maneuvering at a low altitude, the airplane likely had insufficient altitude and time to reestablish fuel flow and restore engine power.