Mechanical & Engine Failure · NTSB CEN13FA509

CESSNA 421C — Paris, IL

1 fatal High-time pilot
DateAugust 27, 2013
LocationParis, IL
AircraftCESSNA 421C
Purpose of flightBusiness
ConditionsDay · Visual Meteorological Cond
Phase / occurrenceTakeoff Loss of engine power (partial)
Pilot age33
Pilot total time8,600 hrs · High time
Time in type2,000 hrs
Fatalities1

Probable cause

The pilot's failure to abort the takeoff during the ground roll after detecting the airplane's degraded performance. Contributing to the accident was the pilot's decision to attempt a flight with a known problem with the left engine and the likely partial loss of left engine power for reasons that could not be determined during the postaccident examination of the engine.

NTSB findings

  • Not determined-Not determined-(general)-(general)-Unknown/Not determined - F
  • Personnel issues-Action/decision-Action-Incorrect action performance-Pilot - C
  • Personnel issues-Action/decision-Info processing/decision-Decision making/judgment-Pilot - F

What happened

Company personnel reported that, in the weeks before the accident, the airplane's left engine had been experiencing a problem that prevented it from initially producing 100 percent power. The accident pilot and maintenance personnel attempted to correct the discrepancy; however, the discrepancy was not corrected before the accident flight, and company personnel had previously flown flights in the airplane with the known discrepancy.

Witnesses reported observing a portion of the takeoff roll, which they described as slower than normal. However, the airplane was subsequently blocked from their view. Examination of the runway environment showed that, during the takeoff roll, the airplane traveled the entire length of the 4,501-ft runway, continued to travel through a 300-ft-long grassy area and a 300-ft-long soybean field, and then impacted the top of 10-ft-tall corn stalks for about 50 ft before it began to climb. About 1/2 mile from the airport, the airplane impacted several trees in a left-wing, nose-low attitude, consistent with the airplane being operated below the minimum controllable airspeed. The main wreckage was consumed by postimpact fire.

Postaccident examinations revealed no evidence of mechanical anomalies with the airframe, right engine, or propellers that would have precluded normal operation. Given the left engine's preexisting condition, it is likely that its performance was degraded; however, postimpact damage and fire preluded a determination of the cause of the problem.

An editorial "what led to it / how to avoid it" analysis for this accident is generated separately and will appear here.

View the official NTSB docket →