Low-Altitude Maneuvering · NTSB CEN15FA154
ROSE THUNDER MUSTANG — Helotes, TX
| Date | February 25, 2015 |
| Location | Helotes, TX |
| Aircraft | ROSE THUNDER MUSTANG (amateur-built) |
| Purpose of flight | Personal |
| Conditions | Day · Visual Meteorological Cond |
| Phase / occurrence | Maneuvering-low-alt flying Collision with terr/obj (non-CFIT) |
| Pilot age | 66 |
| Pilot total time | 3,992 hrs · High time |
| Time in type | 58 hrs |
| Fatalities | 1 |
Probable cause
NTSB findings
- Aircraft-Aircraft oper/perf/capability-Performance/control parameters-Altitude-Not attained/maintained - C
- Personnel issues-Psychological-Attention/monitoring-Monitoring environment-Pilot - C
- Environmental issues-Physical environment-Terrain-(general)-Awareness of condition - C
What happened
A witness observed the airplane flying about 600 ft above ground level over an unpopulated area. He observed the nose of the airplane go straight up while the airplane simultaneously banked left. The airplane became fully inverted and then began to descend in a left bank. The witness reported that he expected to see the airplane pull up and level off at its original altitude and then depart the area as he had seen the airplane do many times before. However, this time, the airplane continued to descend nearly straight down until he lost sight of the airplane behind a hill and trees; he heard a "thud" moments later. He reported that the engine sounded like it was producing full power throughout the maneuver, and he heard no indication of a loss of engine power. The airplane impacted hard, rocky terrain that contained juniper, mesquite, and oak trees. A majority of the fragmented wreckage of the composite airplane was located within 300 ft of the initial impact point; the engine was found about 730 ft from the initial impact point. A postaccident examination of the airframe and engine revealed no evidence of mechanical malfunctions or failures that would have precluded normal operation. An examination of an engine monitoring device installed on the airplane indicated that the engine was producing power at the time of impact. The wreckage path and the length of the debris field indicated that the pilot attempted to recover from the maneuver but was unable to maintain terrain clearance due to the low altitude at which he started the maneuver.