Takeoff & Initial Climb · NTSB CEN15LA059

ROSS H/HERRIOTT M VANS AIRCRAFT RV 3 — Las Cruces, NM

1 fatal High-time pilot
DateNovember 24, 2014
LocationLas Cruces, NM
AircraftROSS H/HERRIOTT M VANS AIRCRAFT RV 3 (amateur-built)
Purpose of flightPersonal
ConditionsDay · Visual Meteorological Cond
Phase / occurrenceTakeoff Loss of control in flight
Pilot age29
Pilot total time1,000 hrs · Experienced
Time in type100 hrs
Fatalities1

Probable cause

The pilot’s failure to maintain airplane control, which resulted in a stall/spin. Contributing to the accident was the pilot’s failure to obtain adequate familiarization in the accident airplane type before the accident.

NTSB findings

  • Personnel issues-Task performance-Use of equip/info-Aircraft control-Pilot - C
  • Personnel issues-Experience/knowledge-Experience/qualifications-Total experience w/ equipment-Pilot - F
  • Aircraft-Aircraft oper/perf/capability-Performance/control parameters-Airspeed-Not attained/maintained - C
  • Aircraft-Aircraft oper/perf/capability-Performance/control parameters-Angle of attack-Not attained/maintained - C

What happened

Several witnesses reported that they observed the airplane make a steep climb shortly after takeoff and that the airplane then made two 90-degree left bank turns to enter the downwind leg of the traffic pattern. During the turns, the airplane's wings were rocking back and forth, the airplane was in a nose-high attitude and not climbing, and the flight control surfaces were moving. The airplane then began another left turn, the left wing dropped, and the airplane spun toward the ground. One witness reported that the engine sounded normal throughout the flight. A friend of the pilot stated that the pilot had purchased the airplane 2 days before the accident and had no previous flight experience in the airplane make and model. He estimated that the pilot had only flown the airplane about 4.0 hours before the accident. Based on witness accounts, there were no preaccident anomalies that would have precluded normal operation. Therefore, it is likely that the pilot lost control of the airplane while maneuvering in the traffic pattern, which resulted in a stall/spin. It is also likely that the pilot's lack of experience in the airplane type contributed to his failure to maintain airplane control during the turns. Although postaccident toxicology tests detected a low level of marijuana in the pilot's blood, liver, and lung, it is unlikely that it impaired his performance on the day of the accident.

An editorial "what led to it / how to avoid it" analysis for this accident is generated separately and will appear here.

View the official NTSB docket →