Mechanical & Engine Failure · NTSB CEN15LA329

O'DELL AEROMASTER — Sulphur Springs, TX

1 fatal Low-time pilot
DateJuly 31, 2015
LocationSulphur Springs, TX
AircraftO'DELL AEROMASTER (amateur-built)
Purpose of flightPersonal
ConditionsDay · Visual Meteorological Cond
Phase / occurrencePrior to flight Aircraft maintenance event
Pilot age46
Pilot total time151 hrs · Low time
Time in type2 hrs
Fatalities1

Probable cause

A total loss of engine power for reasons that could not be determined because postimpact damage precluded a thorough examination of the airplane. Contributing to the accident was the pilot's failure to maintain control following the loss of engine power, which resulted in the airplane exceeding its critical angle of attack and experiencing an aerodynamic stall/spin.

NTSB findings

  • Not determined-Not determined-(general)-(general)-Unknown/Not determined - C
  • Personnel issues-Task performance-Use of equip/info-Aircraft control-Pilot - F
  • Aircraft-Aircraft oper/perf/capability-Performance/control parameters-Pitch control-Not attained/maintained - F
  • Aircraft-Aircraft handling/service-Maintenance/inspections-(general)-Not inspected
  • Aircraft-Aircraft handling/service-Maintenance/inspections-(general)-Not serviced/maintained

What happened

The private pilot had purchased the experimental amateur-built airplane about 2 weeks before the accident. The previous owner had provided the pilot with a 1-hour familiarization flight, during which he repeatedly told the pilot not to lean the mixture control on takeoff. During takeoff on the familiarization flight, the pilot leaned the mixture, resulting in a total loss of engine power while still on the runway. After advancing the mixture control, the engine restarted and they continued the flight. The pilot again leaned the mixture control at altitude, which resulted in the engine running rough.

Following the familiarization flight, the pilot departed to an unknown destination, and, during that flight, he landed at an en route airport due to a rough-running engine. Maintenance personnel at the airport found that the airplane had 26 mechanical discrepancies and was unairworthy. Two mechanics and two experimental aircraft builders told the pilot that the airplane was unsafe and should be taken apart and "trailered" home. The mechanic repaired a leaking brake, replaced all of the spark plugs, serviced the oil, and ran the engine. During the postmaintenance engine run, the magnetos were checked and appeared to function properly, and the engine ran smoothly. The pilot then departed on the accident flight. The mechanic stated that the airplane experienced a total loss of engine power about 200 ft above ground level and the airplane entered a left turn, which subsequently developed into a stall/spin. The airplane completed about 1/4 turn in the spin before impacting terrain.

Postaccident examination was precluded by damage sustained in the postcrash fire. The investigation was unable to determine if the loss of engine power occurred due to the pilot's improper manipulation of the engine controls, or if there was a mechanical malfunction.

An editorial "what led to it / how to avoid it" analysis for this accident is generated separately and will appear here.

View the official NTSB docket →