Fuel Exhaustion & Starvation · NTSB CEN16FA083

CESSNA 172N — Gilmer, TX

1 fatal Low-time pilotNight
DateJanuary 13, 2016
LocationGilmer, TX
AircraftCESSNA 172N
Purpose of flightPersonal
ConditionsNight · Visual Meteorological Cond
Phase / occurrenceApproach Loss of engine power (total)
Pilot age73
Pilot total time259 hrs · Low time
Time in type203 hrs
Fatalities1

Probable cause

The pilot's inadequate preflight planning and inspection, which resulted in a total loss of engine power due to fuel exhaustion. Contributing to the accident was the pilot's failure to maintain an appropriate traffic pattern altitude and distance from the runway, which may have allowed the airplane to glide to the runway following the loss of engine power.

NTSB findings

  • Personnel issues-Task performance-Planning/preparation-Fuel planning-Pilot - C
  • Personnel issues-Task performance-Inspection-Preflight inspection-Pilot - C
  • Aircraft-Fluids/misc hardware-Fluids-Fuel-Fluid level - C
  • Aircraft-Aircraft oper/perf/capability-Performance/control parameters-Altitude-Incorrect use/operation - F
  • Aircraft-Aircraft oper/perf/capability-Performance/control parameters-Descent/approach/glide path-Incorrect use/operation - F
  • Personnel issues-Action/decision-Action-Incorrect action performance-Pilot - F

What happened

The private pilot and one passenger departed on the approximate 35-minute personal flight with an unknown quantity of fuel onboard. Later that evening, they departed to return to their home airport in night visual meteorological conditions without adding additional fuel during their stop. While on final approach to their home airport, the engine lost total power and the airplane impacted trees and terrain. The passenger stated that the engine did not sound any different during the accident flight than on any of the previous flights and that there was no indication of a problem with the airplane when the engine lost power. Postaccident examination of the wreckage revealed no usable fuel within the airplane's fuel system, and no mechanical anomalies that would have precluded normal operation; therefore, it is likely that the airplane experienced a total loss of engine power as a result of fuel exhaustion. While it is unknown what preflight fuel planning the pilot performed and the extent of his preflight inspection, it is apparent that both were inadequate; had he performed both properly, he likely would not have run out of fuel.

Recorded GPS data showed that the pilot flew the traffic pattern 400-600 ft lower than the recommended 1,000-ft above airport elevation and turned to the base leg of the traffic pattern farther from the runway than recommended. Had the pilot flown the traffic pattern at the recommended altitude and distance from the runway, it may have been possible for the airplane to glide to the runway following the loss of engine power.

An editorial "what led to it / how to avoid it" analysis for this accident is generated separately and will appear here.

View the official NTSB docket →