Loss of Control in Flight · NTSB CEN17FA208
Michael S. Logan Kitfox — New Berlin, TX
| Date | June 3, 2017 |
| Location | New Berlin, TX |
| Aircraft | Michael S. Logan Kitfox (amateur-built) |
| Purpose of flight | Personal |
| Conditions | Day · Visual Meteorological Cond |
| Phase / occurrence | Uncontrolled descent Collision with terr/obj (non-CFIT) |
| Pilot age | 60 |
| Pilot total time | 1,138 hrs · Experienced |
| Time in type | 211 hrs |
| Fatalities | 1 |
Probable cause
NTSB findings
- Not determined-Not determined-(general)-(general)-Unknown/Not determined - C
- Aircraft-Aircraft oper/perf/capability-Performance/control parameters-Engine out control-Not attained/maintained - C
- Aircraft-Aircraft oper/perf/capability-Performance/control parameters-Airspeed-Not attained/maintained - C
- Aircraft-Aircraft oper/perf/capability-Performance/control parameters-Angle of attack-Not attained/maintained - C
What happened
The private pilot departed on the local flight to practice touch-and-go takeoffs and landings in the experimental, amateur-built airplane. The airplane impacted flat, open terrain just after takeoff and was consumed by a post-impact fire. There were no witnesses to the accident. The wreckage was confined to a small area, and the orientation of the wreckage was consistent with an aerodynamic stall and spin. Examination of the airframe revealed no evidence of mechanical malfunctions or failures. Engine drive train continuity was established. The propeller blades and spinner did not exhibit evidence of rotation at the time of impact. The damage precluded a thorough examination of the engine ignition system.The pilot's wife said that the pilot had been having ignition issues with the airplane, and described them as the engine missing or quitting entirely during high-powered run-ups. An acquaintance of the pilot reported that the pilot had resolved the ignition problem; however, the pilot did not specify how he had done so. There was no record that the airframe or engine had received a condition inspection in the previous 12 years, and the pilot did not hold a current flight review.
Given the orientation of the wreckage and the lack of rotational signatures on the propeller blades, it is likely that the engine experienced a total loss of power just after takeoff. The reason for the loss of power could not be determined based on the available evidence. Following the loss of power, the pilot failed to maintain adequate airspeed, which resulted in exceeding the airplane's critical angle of attack and a subsequent aerodynamic stall and subsequent spin.