Loss of Control in Flight · NTSB CEN18FA003

SCHAFFER Fisher Horizon 2 — Eden Prairie, MN

1 fatal Low-time pilot
DateOctober 4, 2017
LocationEden Prairie, MN
AircraftSCHAFFER Fisher Horizon 2 (amateur-built)
Purpose of flightPersonal
ConditionsDay · Visual Meteorological Cond
Phase / occurrenceUncontrolled descent Collision with terr/obj (non-CFIT)
Pilot age77
Pilot total time312 hrs · Low time
Time in type0 hrs
Fatalities1

Probable cause

An inflight loss of control and collision with terrain for undetermined reasons after a thorough examination of the airplane's flight controls was unable to confirm control continuity. Contributing to the accident was the pilot's lack of experience in the accident make and model airplane and his lack of recent flight experience.

NTSB findings

  • Personnel issues-Task performance-Use of equip/info-Aircraft control-Pilot - C
  • Aircraft-Aircraft oper/perf/capability-Performance/control parameters-(general)-Not attained/maintained - C
  • Not determined-Not determined-(general)-(general)-Unknown/Not determined - C
  • Personnel issues-Experience/knowledge-Experience/qualifications-Total experience w/ equipment-Pilot - F
  • Personnel issues-Experience/knowledge-Experience/qualifications-Recent experience-Pilot - F

What happened

The private pilot built the airplane over a 24-year period; the accident occurred on the airplane's first flight after the pilot completed building it. The pilot aborted the first takeoff attempt for unknown reasons. During the second takeoff, the airplane was struggling to gain altitude, pitching up and down, and banking. Several witnesses reported hearing "good" engine sounds. Just before the impact, the airplane was in a steep nose-down, left descending spiral before it descended below the trees, followed by a plume of black smoke.

The airplane's wooden structure was mostly destroyed by impact forces and postimpact fire. Portions of the flight control systems were found in the wreckage; however, it could not be determined if they were installed and rigged properly due to the amount of damage. Witnesses reported hearing the engine operating, and postaccident engine examination did not reveal evidence of any mechanical malfunctions or failures that would have precluded normal operation. Therefore, it is unlikely that the airplane experienced a loss of engine power.

The pilot did not have any flight experience in the accident make and model airplane. Further, he had only flown for 4.8 hours in the 12 months before the accident flight. Although it is likely that the pilot's lack of recent flight experience and time in the airplane's make and model played a role in the accident, investigators were unable to determine the cause of the accident due to thermal damage to the airplanes flight controls.

An editorial "what led to it / how to avoid it" analysis for this accident is generated separately and will appear here.

View the official NTSB docket →