Controlled Flight Into Terrain · NTSB CEN19FA161
Cessna 425 — Butler, MO
| Date | June 10, 2019 |
| Location | Butler, MO |
| Aircraft | Cessna 425 |
| Purpose of flight | Personal |
| Conditions | Day · Visual Meteorological Cond |
| Phase / occurrence | Emergency descent Controlled flight into terr/obj (CFIT) |
| Pilot age | 80 |
| Pilot total time | 3,457 hrs · High time |
| Time in type | 1,891 hrs |
| Fatalities | 1 |
Probable cause
NTSB findings
- Aircraft-Aircraft power plant-Engine controls-Power lever-Malfunction
- Aircraft-Aircraft power plant-Engine controls-(general)-Unknown/Not determined
- Personnel issues-Task performance-(general)-(general)-Pilot
- Not determined-Not determined-(general)-(general)-Unknown/Not determined
What happened
During a cross-country flight, the pilot initiated a descent to his intended destination. During the descent, the pilot informed air traffic control (ATC) that he could not retard power on the right engine. Later in the descent, the pilot decided to shut down the right engine. The pilot communicated his desire to land at the nearest airport to ATC, and ATC provided the pilot with the clearance to divert. Radar data showed the airplane in a steady descent toward the airport.
When the airplane was at an altitude of about 2,500 ft mean sea level, the pilot contacted ATC and stated that he was trying to get the airplane under control; radar data showed the airplane in a 360° right turn at the time. The pilot contacted ATC again and stated that he was going to land on a highway. No further transmissions were received from the pilot. After the right turn, the airplane continued in a descent through 1,300 ft mean sea level, at which point radar contact was lost. A witness saw the airplane and stated that the airplane was low and slow but appeared to be in stable flight with both propellers spinning. She did not see any smoke coming from the airplane. She saw the airplane flying northeast to southwest when it suddenly descended nose first into the ground. The airplane impacted a gravel road adjacent to a 100-ft-tall grain silo about 1 mile from the highway and about 3.3 miles from the airport.
Examination of the airframe flight controls, throttle quadrant rigging, and engines revealed no mechanical anomalies. The left and right engine fuel control units (FCU) were disassembled and showed no pre-existing mechanical anomalies that could have prevented normal operation. Some contaminants were found in the Py air sections of both FCUs. According to the manufacturer, if an FCU’s Py bleed was partially restricted with debris, modulation of power could be altered. However, each FCU’s Py bleed had no restrictions or blockages. Examination of the fuel pumps, propeller governors, and overspeed governors of both engines revealed no mechanical anomalies that could have prevented normal operation.
According to the Cessna 425 single-engine performance chart, the airplane could have maintained level flight with one engine inoperative if the landing gear and flaps were retracted and the inoperative engine’s propeller was feathered. At the time of impact, the airplane’s landing gear was extended, the flaps were at 10° down, and the right engine propeller condition lever was about 0.25 inch from minimum and not in the feather detent position.
The reason for the pilot’s reported problem with retarding the right engine’s throttle could not be determined. It is unknown why the pilot made a right turn into the inoperative engine toward the end of the descent, and the reason for the pilot’s loss of control could not be determined.