Loss of Control in Flight · NTSB CEN19FA279
Aero Commander 200 — Howell, MI
| Date | August 20, 2019 |
| Location | Howell, MI |
| Aircraft | Aero Commander 200 |
| Purpose of flight | Personal |
| Conditions | Day · Visual Meteorological Cond |
| Phase / occurrence | Landing Collision with terr/obj (non-CFIT) |
| Pilot age | 64 |
| Pilot total time | 22,974 hrs · High time |
| Time in type | 519 hrs |
| Fatalities | 2 |
Probable cause
NTSB findings
- Aircraft-Aircraft power plant-Power plant-Air intake-Design
- Aircraft-Aircraft handling/service-Maintenance/inspections-(general)-Incorrect service/maintenance
- Aircraft-Aircraft oper/perf/capability-Performance/control parameters-Airspeed-Attain/maintain not possible
- Aircraft-Aircraft oper/perf/capability-Performance/control parameters-Altitude-Attain/maintain not possible
What happened
The single-engine airplane had undergone recent maintenance, including the installation of a fieldoverhauled engine and a three-bladed propeller. The pilot and pilot-rated passenger were conducting a maintenance check flight. One witness reported that the airplane took off normally, but when it reached between about 200 to 300 ft above ground level, it stopped climbing. Another witness reported that he did not hear the engine but that he could not remember whether the propeller was turning.
The accident engine was a modification to the airplane’s original configuration. Such a modification is typically recorded on a Federal Aviation Administration Form 337, “Major Repair and Alternation,” and adopted by a field approval. However, neither the form nor maintenance records regarding the installation of the modified engine were found during the investigation.
A smart phone recorded two videos from inside the airplane. One of the videos captured the accident flight just after takeoff. Several seconds later, a decrease in engine sound was heard, followed by a momentary warning horn. One of the occupants then stated, “we’re stalling,” followed by the sound of the stall warning horn and impact with terrain.
Examination of the airplane revealed substantial damage to the wings and fuselage. During examination of the engine, the air filter element was found displaced and lodged in the intake. The metal screen used to hold the filter element was found improperly installed. The evidence indicates that the improper installation of the metal screen allowed the filter element to become displaced and subsequently lodged in the intake, which blocked the intake air and resulted in a total loss of engine power.