Stall / Spin · NTSB CEN21FA209

MITSUBISHI MU2B — Hattiesburg, MS

3 fatal High-time pilotNightIMCBase-to-final turn
DateMay 5, 2021
LocationHattiesburg, MS
AircraftMITSUBISHI MU2B
Purpose of flightPersonal
ConditionsNight/Dark · Instrument Meteorological Cond
Phase / occurrenceApproach-IFR final approach Aerodynamic stall/spin
Pilot age67
Pilot total time7,834 hrs · High time
Time in type500 hrs
Fatalities3

Probable cause

The pilot’s failure to maintain control of the airplane during the night instrument approach which resulted in an inadvertent aerodynamic stall from which the pilot was unable to recover.

NTSB findings

  • Aircraft-Aircraft oper/perf/capability-Performance/control parameters-Airspeed-Not attained/maintained
  • Personnel issues-Task performance-Use of equip/info-Aircraft control-Pilot

What happened

The pilot was flying a nonprecision approach in instrument meteorological conditions at night. While flying the procedure turn for the approach, the airplane’s speed decayed toward the stall speed before the airplane accelerated back to the standard approach speed. During the descent from the final approach fix, the airplane’s descent stopped for about 30 seconds and then the airplane descended at a rate of about 1,300 ft per minute. The airplane decelerated and continued to descend until the airspeed was about 85 knots (about 7 knots above the calculated stall speed for flaps 20°) and the altitude was 500 ft mean sea level. The last recorded data point showed the airplane about 460 ft mean sea level and 750 ft from the accident site. The airplane impacted a private residence, and a postcrash fire ensued and destroyed the airplane.

Impact signatures were consistent with a low-energy impact. Examination of the airframe and engines did not detect any preimpact anomalies that would have precluded normal operations. Signatures on the engines and propellers were consistent with both engines providing power at impact.

A review of the pilot’s toxicological information found that the level of eszopiclone in his specimens was subtherapeutic and thus not likely a factor in the accident. The circumstances of the accident are consistent with an inadvertent aerodynamic stall from which the pilot was unable to recover.

An editorial "what led to it / how to avoid it" analysis for this accident is generated separately and will appear here.

View the official NTSB docket →