Mechanical & Engine Failure · NTSB ERA10FA074

PIPER PA-28R-200 — Wappinger, NY

2 fatal High-time pilot
DateNovember 22, 2009
LocationWappinger, NY
AircraftPIPER PA-28R-200
Purpose of flightPersonal
ConditionsDay · Visual Meteorological Cond
Phase / occurrenceEmergency descent Off-field or emergency landing
Pilot age52
Pilot total time1,100 hrs · Experienced
Time in typeUnknown
Fatalities2

Probable cause

A total loss of engine power due to a delamination of the No. 3 connecting rod bearing. Contributing to the accident was the inadequate maintenance inspection of the engine oil system.

NTSB findings

  • Aircraft-Aircraft power plant-Engine (reciprocating)-(general)-Failure - C
  • Aircraft-Aircraft power plant-Engine (reciprocating)-Recip engine power section-Damaged/degraded - C
  • Aircraft-Aircraft power plant-Engine (reciprocating)-Recip engine power section-Incorrect service/maintenance - F
  • Personnel issues-Task performance-Maintenance-Scheduled/routine maintenance-Owner/builder - F

What happened

About 10 minutes after takeoff, the pilot advised air traffic control that he was experiencing an oil problem and subsequently maneuvered the airplane for an emergency landing at an airport about 7 nautical miles away. The engine ceased producing power shortly thereafter and the airplane subsequently impacted trees and terrain during a forced landing. Metallurgical examination of the engine components attributed the loss of engine power to the failure of the No. 3 connecting rod bearing. Measurement of journal diameters were consistent with the correct bearings having been installed and a lack of substantial debris in the No. 4 bearing suggested that oil contamination was not contributory. The deformation and color of the recovered No. 3 connecting rod bearing pieces were consistent with the backing of the bearing extruding out of the connecting rod journal interface while under lubrication, and was consistent with failure due to delamination of the bearing. Damage to the bearing from continued operation after it failed prevented a conclusive determination as to whether the bearing had been damaged by a brief period of reduced oil pressure or wear over time. The engine was overhauled about 18 years and 1,700 flight hours prior to the accident. Maintenance records for that period showed inconsistent documentation of manufacturer-recommended oil filter element inspections following engine oil changes, with no documented oil suction screen or filter inspections in the 4 years preceding the accident.

An editorial "what led to it / how to avoid it" analysis for this accident is generated separately and will appear here.

View the official NTSB docket →