Mechanical & Engine Failure · NTSB ERA10FA115
BEECH B-60 — Madison, AL
| Date | January 18, 2010 |
| Location | Madison, AL |
| Aircraft | BEECH B-60 |
| Purpose of flight | Personal |
| Conditions | Day · Visual Meteorological Cond |
| Phase / occurrence | Emergency descent Collision with terr/obj (non-CFIT) |
| Pilot age | 52 |
| Pilot total time | 1,600 hrs · Experienced |
| Time in type | Unknown |
| Fatalities | 2 |
Probable cause
NTSB findings
- Personnel issues-Action/decision-(general)-(general)-Pilot - C
- Aircraft-Aircraft power plant-Engine (reciprocating)-Recip eng cyl section-Failure - F
- Personnel issues-Task performance-Maintenance-Repair-Maintenance personnel
What happened
The multiengine airplane was at an altitude of 6,000 feet when it experienced a catastrophic right engine failure, approximately 15 minutes after takeoff. The pilot elected to return to his departure airport, which was 30 miles away, instead of diverting to a suitable airport that was located about 10 miles away. The pilot reported that he was not able to maintain altitude and the airplane descended until it struck trees and impacted the ground, approximately 3 miles from the departure airport. The majority of the wreckage was consumed by fire. A 5 1/2 by 6-inch hole was observed in the top right portion of the crankcase. Examination of the right engine revealed that the No. 2 cylinder separated from the crankcase in flight. Two No. 2 cylinder studs were found to have fatigue fractures consistent with insufficient preload on their respective bolts. In addition, a fatigue fracture was observed on a portion of the right side of the crankcase, mostly perpendicular to the threaded bore of the cylinder stud. The rear top 3/8-inch and the front top 1/2-inch cylinder hold-down studs for the No. 2 cylinder exceeded the manufacturer's specified length from the case deck by .085 and .111 inches, respectively. The airplane had been operated for about 50 hours since its most recent annual inspection, which was performed about 8 months prior the accident. The right engine had been operated for about 1,425 hours since it was overhauled, and about 455 hours since the No. 2 cylinder was removed for the replacement of six cylinder studs. It was not clear why the pilot was unable to maintain altitude after the right engine failure; however, the airplane was easily capable of reaching an alternate airport had the pilot elected not to return to his departure airport.