Mechanical & Engine Failure · NTSB ERA12LA411

UNIVERSAL STINSON 108 — Portland, ME

1 fatal
DateJune 24, 2012
LocationPortland, ME
AircraftUNIVERSAL STINSON 108
Purpose of flightPersonal
ConditionsDay · Visual Meteorological Cond
Phase / occurrenceEmergency descent Ditching
Pilot age60
Pilot total time504 hrs · Building experience
Time in typeUnknown
Fatalities1

Probable cause

A fatigue failure of the No. 3 piston skirt, which resulted in a total loss of engine power and the subsequent ditching in the ocean.

NTSB findings

  • Aircraft-Aircraft power plant-Engine (reciprocating)-Recip eng cyl section-Fatigue/wear/corrosion - C

What happened

The airplane was flying over the ocean, along the coast at altitudes between 500 to 1,000 feet mean sea level, when the pilot reported a total loss of engine power and indicated that he was not going to be able to glide to the shore. The airplane subsequently impacted water about 100 yards from the shore and sank to a depth of about 70 feet. Postaccident examination of the airplane’s engine revealed that the No. 3 piston skirt fractured, and the resultant debris entered the engine and camshaft gear, affecting the magneto timing. Metallurgical examination of the piston skirt revealed fatigue originating near a machined through-hole. Although the No. 3 piston was overhauled about 5 years before the accident, it was an original piston on the accident engine, which was more than 65 years old.

An editorial "what led to it / how to avoid it" analysis for this accident is generated separately and will appear here.

View the official NTSB docket →