Mechanical & Engine Failure · NTSB ERA13FA256

PIPER PA-32R-300 — Macon, GA

2 fatal High-time pilot
DateMay 27, 2013
LocationMacon, GA
AircraftPIPER PA-32R-300
Purpose of flightPersonal
ConditionsDay · Visual Meteorological Cond
Phase / occurrenceEmergency descent Loss of engine power (total)
Pilot age58
Pilot total time10,050 hrs · High time
Time in type10,050 hrs
Fatalities2

Probable cause

A total loss of engine power due to oil starvation for reasons that could not be determined due to extensive postcrash fire and heat damage to the engine components.

NTSB findings

  • Aircraft-Aircraft power plant-Eng oil sys (airframe furnish)-Pressure-Malfunction - C
  • Aircraft-Aircraft power plant-Engine (reciprocating)-Recip eng oil sys-Failure - C
  • Environmental issues-Physical environment-Terrain-Rough terrain-Contributed to outcome
  • Aircraft-Aircraft power plant-Engine (reciprocating)-Recip eng oil sys-Not serviced/maintained
  • Aircraft-Fluids/misc hardware-Fluids-Oil-Fluid level - C

What happened

A review of air traffic control information revealed that, during the cross-county flight, the pilot requested clearance for a precautionary landing at a nearby airport due to a low oil pressure indication. Shortly after the flight was cleared for landing, the pilot reported that the engine had lost total power. The pilot advised the air traffic controller that he could not make it to the airport and requested to land at a military base that was closer to his current position. The pilot was cleared to land at the military base; however, he never established radio contact with the military base tower. The airplane crashed about 0.8 mile northeast of the base in a heavily wooded swamp, and a postcrash fire ensued.

An examination of the engine revealed that the crankcase was fractured in the areas of the Nos. 4, 5, and 6 cylinders, that the camshaft was fractured, and that the Nos. 4, 5, and 6 connecting rods were separated from the crankshaft. The Nos. 1 and 2 connecting rod bearings and the Nos. 2 and 3 main bearings exhibited wiping, scoring, and extrusion signatures consistent with oil starvation. Although review of maintenance records revealed that Federal Aviation Administration airworthiness directives for the replacement of the oil cooler hose and the oil filter converter plate gasket were not accomplished, extensive postcrash fire and heat damage to the engine components precluded a determination of the cause of the oil starvation.

An editorial "what led to it / how to avoid it" analysis for this accident is generated separately and will appear here.

View the official NTSB docket →