Undetermined · NTSB ERA13LA183
ANDREWS ZODIAC — Collegedale, TN
| Date | March 29, 2013 |
| Location | Collegedale, TN |
| Aircraft | ANDREWS ZODIAC |
| Purpose of flight | Instructional |
| Conditions | Day · Visual Meteorological Cond |
| Phase / occurrence | Prior to flight Ground handling event |
| Pilot age | 77 |
| Pilot total time | 150 hrs · Low time |
| Time in type | 0 hrs |
| Fatalities | 1 |
Probable cause
NTSB findings
- Aircraft-Aircraft systems-Equipment/furnishings-Flight compartment equipment-Incorrect use/operation - C
- Personnel issues-Task performance-Use of equip/info-Use of equip/system-Pilot - C
- Aircraft-Aircraft structures-(general)-(general)-Unintentional use/operation - C
- Personnel issues-Action/decision-Action-Incorrect action performance-Pilot - C
What happened
The pilot had recently purchased the experimental amateur-built airplane and was not familiar with it. The flight instructor reported that, before the pilot's first instructional flight in the airplane, they were unable to start the engine. The pilot unlatched and raised the canopy to call for assistance from ground personnel. As the ground person started to attach the battery charger to the engine, the pilot unbuckled his seatbelt to assist; however, the ground person told the pilot that he did not need to get out of the airplane. The pilot then hastily attempted to refasten his seatbelt, and the pilots lowered the canopy. The flight instructor stated that the canopy appeared to be flush with the fuselage and latched properly; however, about 9 minutes into the flight, the canopy opened, and the airplane entered a negative G dive, at which point, the pilot was pulled out of his seat and the airplane. The flight instructor remained in his seat with the seatbelt fastened and landed the airplane uneventfully. Examination of the pilot's seatbelt and the canopy latch did not reveal any malfunctions or failures that would have precluded normal operation. Therefore, it is likely that the pilots did not latch the canopy properly before takeoff and that the pilot did not properly fasten his seatbelt, which allowed him to be pulled from the airplane due to the high G forces after the canopy opened in flight.