Mechanical & Engine Failure · NTSB ERA15FA378
PIPER PA 30 — St. Petersburg, FL
| Date | September 30, 2015 |
| Location | St. Petersburg, FL |
| Aircraft | PIPER PA 30 |
| Purpose of flight | Personal |
| Conditions | Day · Visual Meteorological Cond |
| Phase / occurrence | Initial climb Loss of engine power (total) |
| Pilot age | 24 |
| Pilot total time | 768 hrs · Building experience |
| Time in type | 0 hrs |
| Fatalities | 1 |
Probable cause
NTSB findings
- Personnel issues-Task performance-Use of equip/info-Aircraft control-Pilot - C
- Aircraft-Aircraft oper/perf/capability-Performance/control parameters-Airspeed-Not attained/maintained - C
- Aircraft-Aircraft power plant-Engine (reciprocating)-Recip engine power section-Malfunction - C
- Aircraft-Aircraft systems-Indicating/recording systems-Instrument panel-Incorrect service/maintenance - F
- Personnel issues-Task performance-Maintenance-Installation-Maintenance personnel - F
What happened
The commercial pilot, who had no documented previous experience in the make and model multiengine airplane, was performing touch-and-go landings on a 9,730-ft-long runway to familiarize himself with the airplane. Witnesses reported that, during the second takeoff, the airplane appeared to "struggle." Another witness reported the airplane was climbing at an unusually shallow angle. The airplane then drifted to the right of the runway centerline, rolled sharply to the right, and descended to ground impact in a steep, nose-low attitude. The airplane came to rest about 180 ft right of the runway centerline and about 1,450 ft before the end of the runway's paved surface.
Examination of the wreckage revealed that the right engine throttle was retarded, and the propeller lever was in the feather position. The right propeller blades displayed little damage and appeared to be in the feathered position. The left engine throttle and propeller levers were full forward, and damage to the left propeller was indicative of full left engine power at impact. Examination of the right engine revealed three anomalies; the diaphragm of the right fuel servo exhibited an unusual soot pattern; particulate contamination was in the fuel filter screen; and the spark plugs were in a degraded condition. However, none of these anomalies would likely have resulted in a total loss of engine power.
Based on the witness descriptions and the lack of damage to the right propeller blades, it is likely that during the climb, the right engine experienced, at least, a partial loss of power. Based on the postaccident positions of the right engine throttle and propeller levers and signatures observed on the right engine's propeller, the pilot likely responded to the loss of right engine power by retarding the right throttle and feathering the right propeller; however, he did not maintain the appropriate airspeed and subsequently lost control of the airplane. Given the airplane's impact location about 1,450 ft before the end of the runway, it is likely that, if the pilot had immediately retarded both throttles, maintained the appropriate airspeed, and landed straight ahead, he likely would have maintained control of the airplane. Additionally, the airspeed indicator did not have a marking for single-engine minimum controllable airspeed, nor was there a placard on the instrument panel as required by a Federal Aviation Administration airworthiness directive and the airplane flight manual. While the lack of these markings was not causal to the accident, their presence might have reminded the pilot of this critical information, and might have changed the outcome of the event.