Fuel Exhaustion & Starvation · NTSB ERA15LA149
PIPER PA-24-250 — Fort Myers, FL
| Date | March 9, 2015 |
| Location | Fort Myers, FL |
| Aircraft | PIPER PA-24-250 |
| Purpose of flight | Personal |
| Conditions | Day · Visual Meteorological Cond |
| Phase / occurrence | Emergency descent Off-field or emergency landing |
| Pilot age | 59 |
| Pilot total time | 410 hrs · Building experience |
| Time in type | 11 hrs |
| Fatalities | 1, 1 serious |
Probable cause
NTSB findings
- Aircraft-Aircraft systems-Fuel system-Fuel selector/shutoff valve-Unintentional use/operation - C
- Personnel issues-Task performance-Use of equip/info-Use of equip/system-Pilot - C
- Aircraft-Fluids/misc hardware-Fluids-Fuel-Fluid level - C
What happened
The pilot reported that, about 10 miles from the destination airport, he switched the left and right fuel tanks from the auxiliary position to the main tank position. On final approach for landing and when the airplane was at an altitude of about 500 ft, the engine stopped producing power. The propeller continued to rotate, but the engine did not respond to throttle inputs. The pilot stated that he then switched the fuel selectors from the main tank position back to the auxiliary tank position and turned on the electric fuel boost pumps, but the engine did not regain power. He added that, each time he moved the fuel selectors, he visually confirmed their position. The pilot performed a forced landing to a parking lot, during which the airframe aft of the engine compartment was fractured and the fuselage was substantially damaged. There was no odor of fuel or evidence of fuel spillage at the accident scene; however, the fuel caps were removed, and large quantities of fuel were found in each wing tank.
Examination of the cockpit revealed that both the left and right tank fuel selectors were in the "off" position and that the fuel selector position decal had been displaced upward and over each handle by impact forces, which indicates that the fuel selectors were in the "off" position at impact and not moved subsequently. Continuity of the fuel system was confirmed from all four fuel tanks, through the fuel selectors, to the fuel supply line forward of the firewall. The engine was test run, and it started immediately, accelerated smoothly, and ran without interruption at all power settings.