Low-Altitude Maneuvering · NTSB ERA17FA088

SHARPE WILLIAM L BUCCANEER II B — Mayo, FL

1 fatal High-time pilotLow altitude
DateJanuary 14, 2017
LocationMayo, FL
AircraftSHARPE WILLIAM L BUCCANEER II B (amateur-built)
Purpose of flightPersonal
ConditionsDay · Visual Meteorological Cond
Phase / occurrenceManeuvering-low-alt flying Collision with terr/obj (non-CFIT)
Pilot age61
Pilot total time8,000 hrs · High time
Time in typeUnknown
Fatalities1

Probable cause

The pilot's failure to see and avoid power lines while flying at low altitude.

NTSB findings

  • Personnel issues-Psychological-Attention/monitoring-Monitoring environment-Pilot - C
  • Personnel issues-Action/decision-Info processing/decision-Identification/recognition-Pilot - C
  • Environmental issues-Physical environment-Object/animal/substance-Wire-Awareness of condition - C

What happened

The sport pilot of the experimental, amateur-built, amphibious airplane flew to meet a friend to camp for the night along a river. He landed on the river to the north, flying over power lines during the landing approach, and pulled the airplane onto the shore. The pilot offered to help his friend search for a life vest that had floated downstream after he finished unloading the gear from the airplane. Multiple witnesses watched as the pilot departed northbound on the river, made a 180° turn southbound, then flew over the river, beneath treetop level, and out of sight. They reported hearing a loud "boom" and the engine noise stop just before a power outage occurred. One witness reported seeing the airplane flying 30-40 ft above the river when it "suddenly flipped backwards and then hit the water." One witness reported that the sky was grey and overcast, and that the sun was setting about the time of the accident, making the power lines difficult to see. The powerlines directly overhead of the accident site displayed striations consistent with the airplane impacting the powerlines.

Examination of the wreckage revealed no evidence of a preexisting anomaly or malfunction that would have precluded normal operation. Toxicology testing on the pilot detected two medications, which were unlikely to have caused impairment, and the autopsy revealed an enlarged heart; however, there was no evidence of a heart attack or any other incapacitating event. It is likely that, while flying along the river at low altitude, the pilot failed to see the powerlines, which resulted in an in-flight collision with the powerlines and impact with the river.

An editorial "what led to it / how to avoid it" analysis for this accident is generated separately and will appear here.

View the official NTSB docket →