Stall / Spin · NTSB ERA19FA036

Titan TORNADO 1 — Louisa, VA

1 fatal
DateNovember 4, 2018
LocationLouisa, VA
AircraftTitan TORNADO 1 (amateur-built)
Purpose of flightPersonal
ConditionsDay · Visual Meteorological Cond
Phase / occurrenceInitial climb Aerodynamic stall/spin
Pilot age70
Pilot total time613 hrs · Building experience
Time in type48 hrs
Fatalities1

Probable cause

The pilot's failure to maintain airspeed and the airplane's exceedance of its critical angle of attack, which resulted in an aerodynamic stall and spin at a low altitude.

NTSB findings

  • Personnel issues-Task performance-Use of equip/info-Aircraft control-Pilot - C
  • Aircraft-Aircraft oper/perf/capability-Performance/control parameters-Angle of attack-Not attained/maintained - C
  • Aircraft-Aircraft oper/perf/capability-Performance/control parameters-Airspeed-Not attained/maintained - C

What happened

The pilot of the experimental amateur-built airplane took off and made a left turn to travel north of the airport. A witness at the airport reported that the airplane sounded louder than normal during departure. About 1 minute 18 seconds after takeoff, the airplane climbed to an altitude of about 400 feet above ground level at a groundspeed of 60 knots. During the next 22 seconds, the airplane descended about 300 ft and slowed to a groundspeed of 34 knots before impacting a field. The lack of a discernable debris path, asymmetric damage to both wings, and the airplane's relatively low ground speed immediately before the accident all suggest that the airplane likely departed controlled flight after entering an aerodynamic stall and spin.

Examination of the engine revealed no preimpact mechanical malfunctions that would have precluded the engine from operating normally. The muffler had a hole measuring about 2 inches in diameter where the muffler rear mount attached to the engine. Although the pilot had a headset, if the separation of the muffler had occurred during the accident flight, the increased engine noise due to the hole in the muffler could have distracted the him, and resulted in his subsequent loss of control and an aerodynamic stall/spin.

The pilot had longstanding hypertensive cardiomyopathy, which could have increased his risk of an arrhythmia that could have caused palpitations, shortness of breath, anxiety, and/or fainting. However, the pilot's medications may have mitigated that risk. Therefore, the investigation could not determine from the available information whether the pilot's heart disease contributed to the circumstances of the accident.

An editorial "what led to it / how to avoid it" analysis for this accident is generated separately and will appear here.

View the official NTSB docket →