Mechanical & Engine Failure · NTSB ERA19FA164

Piper PA28 — Foley, AL

1 fatal
DateMay 6, 2019
LocationFoley, AL
AircraftPiper PA28
Purpose of flightInstructional
ConditionsDay · Visual Meteorological Cond
Phase / occurrenceInitial climb Loss of engine power (partial)
Pilot age22
Pilot total time978 hrs · Building experience
Time in type507 hrs
Fatalities1, 1 serious

Probable cause

A partial loss of engine power due to a stuck exhaust valve and the flight instructor's exceedance of the airplane's critical angle of attack following the loss of power, which resulted in an aerodynamic stall at low altitude.

NTSB findings

  • Aircraft-Aircraft power plant-Engine (reciprocating)-Recip eng cyl section-Failure - C
  • Personnel issues-Task performance-Use of equip/info-Aircraft control-Instructor/check pilot - C
  • Aircraft-Aircraft oper/perf/capability-Performance/control parameters-Angle of attack-Not attained/maintained - C

What happened

The flight instructor and student pilot were conducting simulated engine-out emergency procedures in the airport traffic pattern. About 300-400 ft above ground level after takeoff, witnesses reported that the flight instructor announced on the radio that the engine had quit. Witnesses reported that the airplane then entered a nose-high, steep left turn before pitching down and impacting the ground.

Postaccident examination of the airframe and flight controls revealed no mechanical anomalies that would have precluded normal operation. Examination of the engine revealed that the No. 4 cylinder exhaust valve was stuck in the valve guide due to excessive combustion deposits. It is likely that the stuck exhaust valve resulted in a partial loss of engine power.

A flight instructor who flew the accident airplane the day before the accident flight reported experiencing engine roughness when performing simulated engine-out procedures. Following that flight, a mechanic cleaned the sparkplugs, performed an engine run-up, and returned the airplane to service; however, maintenance records did not show that the engine valves were inspected for sticking at that time. Manufacturer service instructions suggested inspecting for valve sticking at regular intervals or sooner if sticking was suspected. If a valve inspection had been completed in accordance with engine manufacturer guidance the day before the accident following the report of engine roughness, it is likely that the heavy carbon deposits on the exhaust valve would have been detected.

Given that the flight instructor reportedly had students trim the airplane nose-up when landing, it is possible that the airplane was trimmed nose-high at the time of takeoff and the subsequent loss of engine power. Such a trim setting would have led to excessive pitch up, resulting in a rapid loss of airspeed, an exceedance of the airplane's critical angle of attack, and an aerodynamic stall at low altitude.

An editorial "what led to it / how to avoid it" analysis for this accident is generated separately and will appear here.

View the official NTSB docket →