Fuel Exhaustion & Starvation · NTSB ERA21FA010

CZECH SPORT CRUISER — Waterloo, AL

1 fatal
DateOctober 7, 2020
LocationWaterloo, AL
AircraftCZECH SPORT CRUISER
Purpose of flightPersonal
ConditionsDay · Visual Meteorological Cond
Phase / occurrenceEmergency descent Collision with terr/obj (non-CFIT)
Pilot age69
Pilot total time400 hrs · Building experience
Time in type400 hrs
Fatalities1

Probable cause

The improper configuration of the airplane’s fuel system, which resulted in a total loss of engine power due to fuel starvation following the failure of the electric fuel pump.

NTSB findings

  • Aircraft-Fluids/misc hardware-Fluids-Fuel-Incorrect service/maintenance
  • Aircraft-Aircraft systems-Fuel system-Fuel pumps-Failure
  • Aircraft-Aircraft systems-Fuel system-Fuel distribution-Incorrect use/operation
  • Personnel issues-Task performance-Maintenance-Installation-Pilot
  • Personnel issues-Task performance-Maintenance-Modification/alteration-Pilot
  • Aircraft-Fluids/misc hardware-Misc hardware-Hoses and tubes-Not installed/available

What happened

According to the pilot’s spouse, he departed on the morning of the accident to return home from a cross-country trip. A search was initiated when the pilot did not return as expected, and the airplane was found in a heavily wooded area about 45 nautical miles from an intermediate airport where the pilot had stopped to refuel.

Examination of the airplane revealed no anomalies with the flight controls and the examination of the engine did not reveal any anomalies that would have precluded normal operation. An examination of the fuel system revealed that an aftermarket electric automotive fuel pump was used in place of the recommended manufacturer’s fuel pump. The fuel pump was removed and connected directly to a 12-volt power source, and it did not operate. This type of fuel pump did not allow fuel bypass in the event of failure. According to the engine manufacturer’s fuel system installation instructions and a safety directive published by the airframe manufacturer, a bypass fuel line should be installed in the event of failure of the electric fuel pump, in order to enable a continuous supply of fuel to the engine.

Based on the available information, it is likely that the pilot experienced a total loss of engine power due to fuel starvation following the failure of the electric fuel pump. Also causal was the pilot’s decision to install the electric fuel pump with no bypass fuel line, contrary to published guidance from the airframe and engine manufacturers.

An editorial "what led to it / how to avoid it" analysis for this accident is generated separately and will appear here.

View the official NTSB docket →