Mechanical & Engine Failure · NTSB ERA21LA080
SOCATA TB10 — Pembroke Pines, FL
| Date | December 17, 2020 |
| Location | Pembroke Pines, FL |
| Aircraft | SOCATA TB10 |
| Purpose of flight | Personal |
| Conditions | Day · Visual Meteorological Cond |
| Phase / occurrence | Landing-flare/touchdown Off-field or emergency landing |
| Pilot age | 37 |
| Pilot total time | 236 hrs · Low time |
| Time in type | 36 hrs |
| Fatalities | 1, 3 serious |
Probable cause
NTSB findings
- Environmental issues-Conditions/weather/phenomena-Temp/humidity/pressure-Conducive to carburetor icing-Effect on equipment
- Aircraft-Aircraft systems-Ice/rain protection system-Intake anti-ice, deice-Not used/operated
- Personnel issues-Action/decision-Action-Lack of action-Pilot
- Personnel issues-Action/decision-Info processing/decision-Identification/recognition-Pilot
What happened
The pilot was initiating a cross country flight with three passengers on board. After performing an engine run-up that included a functional check of the carburetor heat and verification of full static rpm, he waited 8 minutes for his instrument takeoff clearance with the engine operating about 1,200 rpm. After being cleared for takeoff, he taxied onto the runway, applied full throttle, and began his takeoff roll. One pilot-rated witness, who was also an airframe and powerplant mechanic, reported hearing a loud noise that he described as a “definite hard miss,” and a second pilot-rated witness reported hearing “popping and banging” throughout the airplane’s takeoff. The pilot reported attaining a normal takeoff distance, which would have been about 1,135 ft according to performance calculations; however, the second witness noted the airplane rotated about 1,542 ft down the 3,350-ft-long runway.
After rotating, the pilot pitched for 73 knots, and at 100 ft, he reported the airplane would not climb. The airspeed started to decrease, which resulted in the stall warning horn sounding. With a significant loss of engine power, he attempted to maintain 70 knots but was unable, and he made small pitch adjustments to stay above 65 knots, eventually retracting the flaps. Unable to maintain altitude, he maneuvered for an off-airport forced landing during which the airplane impacted a tree and then the ground. A postcrash fire erupted. The pilot exited the burning airplane but returned to rescue the right front and left rear seat passengers (both minors) who were unable to release their restraints for undetermined reasons.
Although the pilot reported the fuel selector was on the right fuel tank, it was found selected to the left fuel tank; however, this likely did not contribute to the partial loss of engine power as both tanks were fueled before the flight. Examination of the engine, engine systems, and the remains of the left and right fuel supply and vent systems revealed no evidence of any preimpact mechanical malfunctions or failures that would have precluded normal operation.
The atmospheric conditions at the time of the accident were conducive to the development of serious carburetor icing at glide power. Given the evidence, it is likely that following the prolonged wait with the engine at a low power setting before takeoff, the engine developed carburetor ice during the subsequent takeoff, which resulted in the partial loss of engine power during takeoff.
Although the pilot reported a normal rotation point, the witness-reported rotation point and onboard recorded data showed the airplane’s takeoff roll was between 34% to 41% longer than the calculated takeoff roll distance for the environmental conditions that day. The longer takeoff roll and the abnormal engine noises reported by the witnesses should have alerted the pilot to the partial loss of engine power and prompted him to abort the takeoff, which would have avoided the accident.