Stall / Spin · NTSB ERA22FA384

MXR TECHNOLOGIES MX2 — Osteen, FL

2 fatal High-time pilotLow altitude
DateAugust 24, 2022
LocationOsteen, FL
AircraftMXR TECHNOLOGIES MX2 (amateur-built)
Purpose of flightOther Work Use
ConditionsDay · Visual Meteorological Cond
Phase / occurrenceManeuvering-aerobatics Aerodynamic stall/spin
Pilot age61
Pilot total time1,342 hrs · Experienced
Time in typeUnknown
Fatalities2

Probable cause

The pilot’s loss of airplane control while performing aerobatic maneuvers, which resulted in the airplane entering an inverted flat spin that continued until the airplane impacted terrain.

NTSB findings

  • Personnel issues-Task performance-Use of equip/info-Aircraft control-Pilot
  • Aircraft-Aircraft oper/perf/capability-Performance/control parameters-(general)-Not attained/maintained

What happened

The accident flight was part of a training and demonstration flight that included a series of aerobatic maneuvers. Flight track data for the accident flight revealed that the airplane departed and maneuvered for about 7 minutes before impacting terrain almost directly under the last data point. No linear ground scar was observed at the accident site, which was indicative of the airplane having descended nearly vertically to ground impact. Additionally, the wreckage was found in an inverted orientation. Examination of the wreckage revealed no evidence of a preimpact mechanical anomaly that would have precluded normal operation of the airplane structure, the flight controls, or the engine. Estimated weight and balance calculations revealed that the airplane’s weight and its aft center of gravity were likely at or near the limit for aerobatic flight.

Given the purpose of the flight, the flight track, and the orientation of the wreckage, it is likely that the pilot lost control of the airplane while performing aerobatic maneuvers and that the airplane inadvertently entered an inverted flat spin. A fracture of the elevator torque tube at the aft bulkhead opening corresponded with the elevator control surface being in the full noseup position when the airplane impacted the ground, which would have been a position consistent with the pilot attempting to recover from an inverted flat spin. The airplane’s weight and aft center of gravity likely contributed to the pilot’s inability to recover from the spin. Thus, the inverted flat spin likely continued until the airplane impacted terrain.

Toxicology testing revealed subtherapeutic concentration of chlorpheniramine in the pilot’s blood, which likely did not cause significant symptoms. Hydrocodone and its active metabolites (hydromorphone and dihydrocodeine) were detected in the pilot’s urine but not in his blood, so they would not have had any therapeutic effect or side effect. Thus, the detected chlorpheniramine, hydrocodone, hydromorphone, and dihydrocodeine did not contribute to this accident.

An editorial "what led to it / how to avoid it" analysis for this accident is generated separately and will appear here.

View the official NTSB docket →