Landing / Ground Loss of Control · NTSB LAX08FA092
BEECH 95-B55 — Benson, AZ
| Date | April 3, 2008 |
| Location | Benson, AZ |
| Aircraft | BEECH 95-B55 |
| Purpose of flight | Business |
| Conditions | Night · Visual Meteorological Cond |
| Phase / occurrence | Landing-flare/touchdown Hard landing |
| Pilot age | 53 |
| Pilot total time | 274 hrs · Low time |
| Time in type | 29 hrs |
| Fatalities | 2 |
Probable cause
NTSB findings
- Aircraft-Aircraft oper/perf/capability-Performance/control parameters-Lateral/bank control-Not attained/maintained - C
- Aircraft-Aircraft oper/perf/capability-Performance/control parameters-Descent/approach/glide path-Not attained/maintained - C
- Personnel issues-Task performance-Use of equip/info-Aircraft control-Pilot - C
- Personnel issues-Experience/knowledge-Experience/qualifications-Total experience w/ equipment-Pilot - F
- Environmental issues-Conditions/weather/phenomena-Light condition-Dark-Not specified - F
What happened
A witness at the airport reported that the airplane's first approach for landing in dark night conditions appeared high and fast. Prior to touchdown, the pilot announced over the common traffic frequency that he was going around. During the second approach, which the witness reported as not as high and fast as the first approach, the airplane was about 10 feet above ground level when it passed the midfield point on the 4,000-foot runway. The witness lost sight of the airplane behind a hangar, but heard what sounded like a hard landing, followed by the sound of increasing engine sounds. The witness looked over the hangars and saw a green light (right wing tip) arc to the left as if the airplane were rolling inverted. The airplane collided with the ground in a near-inverted, slightly nose-down attitude and came to rest between the runway and the taxiway. Postcrash examination of the airframe and flight control systems found no anomalies. The left engine was examined and subsequently placed in a test cell. The engine started easily and ran smoothly at various rated power settings. The right engine was subject to a teardown inspection. The disassembly of the engine did not reveal any preexisting anomalies that would have precluded normal operation of the engine. Both propellers had impact marks on the spinner from contact with a counterweight while the blade/counterweight was at a low pitch position. There were no impact marks or other indications to suggest that either propeller was feathered. Both propellers were turning and were driven toward a lower blade angle at impact as evidenced by the damage to the low pitch stop. A review of the private pilot's flight logbook indicated the pilot had accumulated approximately 274 hours total flight time in all aircraft, with only 29 hours in the aircraft type and 5 hours of night flying experience logged.