Loss of Control in Flight · NTSB WPR09LA384

BOEING E75 — Happy Jack, AZ

1 fatal
DateAugust 4, 2009
LocationHappy Jack, AZ
AircraftBOEING E75
Purpose of flightPersonal
ConditionsDay · Visual Meteorological Cond
Phase / occurrenceUncontrolled descent Collision with terr/obj (non-CFIT)
Pilot age70
Pilot total time668 hrs · Building experience
Time in typeUnknown
Fatalities1, 1 serious

Probable cause

The pilot's failure to maintain airspeed while maneuvering which resulted in an inadvertent stall/spin. Contributing to the accident was the high density altitude.

NTSB findings

  • Aircraft-Aircraft oper/perf/capability-Performance/control parameters-Airspeed-Not attained/maintained - C
  • Personnel issues-Task performance-Use of equip/info-Aircraft control-Pilot - C
  • Environmental issues-Conditions/weather/phenomena-Temp/humidity/pressure-High density altitude-Effect on equipment

What happened

The passenger reported that during cruise flight, the pilot “decided to turn around because the airplane was not gaining altitude.” The passenger stated that his head was down looking at a chart as they turned and when he looked up, “they were going down fast and then he blacked out.” Examination of the accident site and airplane by first responders revealed that the airplane impacted the ground within an open field at an elevation of about 6,692 feet mean sea level (msl). Structural damage was observed to the upper and lower left wings and empennage consistent with a stall and a nose down impact. Using reported weather conditions from a weather reporting station located 15 miles northwest of the accident site and the reported accident site elevation, density altitude was calculated to be about 10,681 feet msl. Post accident examination of the recovered airframe and engine revealed no mechanical anomalies that would have precluded normal operation.

An editorial "what led to it / how to avoid it" analysis for this accident is generated separately and will appear here.

View the official NTSB docket →