Stall / Spin · NTSB WPR11FA428

VEATCH KITFOX — Caldwell, ID

2 fatal Low-time pilot
DateSeptember 4, 2011
LocationCaldwell, ID
AircraftVEATCH KITFOX (amateur-built)
Purpose of flightPersonal
ConditionsDay · Visual Meteorological Cond
Phase / occurrenceInitial climb Aerodynamic stall/spin
Pilot age69
Pilot total time305 hrs · Low time
Time in type162 hrs
Fatalities2

Probable cause

The pilot’s failure to prevent a low-altitude stall and spin following a complete loss of engine power during the initial climb after takeoff.

NTSB findings

  • Aircraft-Aircraft power plant-Engine (reciprocating)-(general)-Failure - C
  • Aircraft-Aircraft oper/perf/capability-Performance/control parameters-Pitch control-Not attained/maintained - C
  • Personnel issues-Task performance-Use of equip/info-Aircraft control-Pilot - C

What happened

The builder/owner/pilot of the kit-built experimental airplane and his non-pilot-rated passenger flew from California to Idaho in order to attend the kit manufacturer's fly-in and visit relatives. Two days before the accident, they flew to Idaho, and the next day they flew 4 hours. On the third day, the airplane was taxied from its parking spot on the ramp about 0740, and the pilot conducted a takeoff to about 50 feet, before landing straight ahead on the remaining runway. The investigation was unable to determine the purpose of this flight, or whether the passenger was on board at that time. The airplane was then taxied back to the ramp. About 13 minutes later, the airplane left the ramp again, taxied to the opposite runway, and began another takeoff roll. When the airplane was about 200 feet above the runway, the engine stopped developing power. The airplane stalled and spun to the ground, impacting on airport property near the departure end of the runway.

Weight and balance calculations indicated that the airplane was likely 60 to 100 pounds above its maximum allowable weight, and that the center of gravity was about 1.7 inches forward of the aft limit, which would have increased the airplane pitch up tendency following the loss of engine power. Because the airplane was experimental and the pitch trim setting was unable to be determined during postaccident examination, the investigation was unable to determine whether there was sufficient control authority to prevent the stall and also what the required control forces would have been.

Examination of the wreckage revealed that the two installed air filters had flow capacities well below the minimum value specified by the engine manufacturer, which would have limited the engine's ability to develop its full rated power. However, this was not a factor in this accident, because the airplane had been flown successfully in the previous days.

The engine was not equipped with carburetor heat, even though it was required by the engine manufacturer. When plotted on a carburetor icing chart, the ambient air temperature and dew point values indicated that conditions for serious carburetor icing at cruise power existed. The engine-driven fuel pump was too damaged to test, but the engine manufacturer noted that it should have been replaced in accordance with a 2007 Service Bulletin, which warned that excessively high fuel pressure could result in "engine malfunction and/or massive fuel leakage." Although the possibility exists that the engine experienced a total loss of power due to carburetor icing, excessive fuel pressure, or a combination of the two, the investigation was unable to conclusively determine whether either caused the loss of engine power.

Finally, no evidence of an angle-of-attack or stall warning system was observed in the wreckage. Although not required, such a system might have alerted the pilot of the impending stall and helped him avoid the stall and subsequent spin.

An editorial "what led to it / how to avoid it" analysis for this accident is generated separately and will appear here.

View the official NTSB docket →