Mechanical & Engine Failure · NTSB WPR11LA183
TOMEI S12 XL — Pleasant Grove, CA
| Date | April 3, 2011 |
| Location | Pleasant Grove, CA |
| Aircraft | TOMEI S12 XL |
| Purpose of flight | Personal |
| Conditions | Day · Instrument Meteorological Cond |
| Phase / occurrence | Takeoff Loss of engine power (total) |
| Pilot age | 53 |
| Pilot total time | 165 hrs · Low time |
| Time in type | 165 hrs |
| Fatalities | 1 |
Probable cause
NTSB findings
- Aircraft-Aircraft power plant-Engine (reciprocating)-Recip eng cyl section-Malfunction - C
- Personnel issues-Action/decision-Action-Incomplete action-Pilot - C
- Personnel issues-Task performance-Planning/preparation-(general)-Pilot - C
- Aircraft-Aircraft oper/perf/capability-Performance/control parameters-Airspeed-Not attained/maintained - C
- Personnel issues-Task performance-Use of equip/info-Aircraft control-Pilot - C
What happened
A pilot-rated witness said that the airplane was airborne within “a couple of minutes” after the engine was started and that, when the airplane reached an altitude of 200 to 300 feet above the ground during climb out, it appeared to slow. The witness said that the airplane then banked left and descended in a spiral until it impacted the ground. Postaccident examination of the engine revealed evidence of abnormal piston wear and cylinder damage, including mechanical scoring and vertical grooves along the forward cylinder walls and piston skirt. A representative of the engine manufacturer reported that the observed cylinder and piston damage was consistent with an in-flight cold seizure of the piston (a condition where the piston seizes within the cylinder). About 17 years before the accident, the engine manufacturer issued a Service Information Letter (SIL) that addressed the potential for such a piston seizure. The SIL stated in part “...Putting a cold engine to hard work without uniform and correct warm up will cause the piston to expand quicker than the cylinder, minimizing clearance and creating piston scuffing and seizure.” It is likely that the pilot did not allow enough time for the engine to warm up before taking off.