Fuel Exhaustion & Starvation · NTSB WPR12FA001
VAUGHN PULSAR — West Jordan, UT
| Date | October 4, 2011 |
| Location | West Jordan, UT |
| Aircraft | VAUGHN PULSAR (amateur-built) |
| Purpose of flight | Personal |
| Conditions | Day · Visual Meteorological Cond |
| Phase / occurrence | Initial climb Aerodynamic stall/spin |
| Pilot age | 28 |
| Pilot total time | 2,100 hrs · Experienced |
| Time in type | Unknown |
| Fatalities | 2 |
Probable cause
NTSB findings
- Aircraft-Aircraft oper/perf/capability-Performance/control parameters-Airspeed-Not attained/maintained - C
- Personnel issues-Task performance-Use of equip/info-Aircraft control-Pilot - C
- Environmental issues-Conditions/weather/phenomena-Temp/humidity/pressure-High density altitude-Contributed to outcome
- Aircraft-Aircraft oper/perf/capability-Aircraft capability-Maximum weight-Capability exceeded - C
- Personnel issues-Action/decision-Action-Incorrect action performance-Maintenance personnel - C
- Aircraft-Aircraft power plant-Engine fuel and control-Fuel control/carburetor-Incorrect service/maintenance - C
- Personnel issues-Task performance-Planning/preparation-Weight/balance calculations-Pilot
What happened
On the morning of the accident, the pilot and the new owner arrived at the airport to pick up the airplane. The previous owner saw that their total weight was greater than he had been told during an earlier inquiry and advised the flight instructor and the new owner that their total weight might put the airplane near its maximum allowable gross weight. He also advised them not to add any more fuel than was already onboard, and then handed them the weight and balance sheet for the airplane. Subsequently, witnesses saw the airplane take off and ascend at an extremely low rate of climb. When another pilot waiting to take off asked whether they were having any technical difficulties, the accident pilot responded that there was nothing wrong but that it was just a “weak airplane.” About 1/2 mile after passing the departure end of the runway, the pilot initiated a right turn but failed to maintain sufficient airspeed, resulting in the airplane stalling and descending into the terrain. The postaccident investigation determined that the airplane was being operated above its maximum allowable gross weight and that it was being operated in a density altitude that was 2,120 feet higher than the field elevation. An engine teardown examination determined that both of its carburetors had jet needles installed that produced a richer-than-normal fuel-air mixture. This was due to an incorrect reassembly after an overhaul of the carburetors. The weight of the airplane, the high density altitude, and the overly rich fuel-air mixture most likely combined to significantly reduce the performance of the airplane.