Undetermined · NTSB WPR12LA302

BUNCH COZY-CANARDIII — Winslow, AZ

1 fatal Low-time pilot
DateJuly 11, 2012
LocationWinslow, AZ
AircraftBUNCH COZY-CANARDIII (amateur-built)
Purpose of flightPersonal
ConditionsDay · Visual Meteorological Cond
Phase / occurrencePrior to flight Aircraft loading event
Pilot age65
Pilot total time239 hrs · Low time
Time in typeUnknown
Fatalities1, 1 serious

Probable cause

The pilot’s failure to maintain airplane control during climb in high-density altitude conditions and with the airplane’s weight in excess of its maximum allowable gross weight.

NTSB findings

  • Personnel issues-Task performance-Use of equip/info-Aircraft control-Pilot - C
  • Aircraft-Aircraft oper/perf/capability-Performance/control parameters-Pitch control-Not attained/maintained - C
  • Aircraft-Aircraft oper/perf/capability-Aircraft capability-Maximum weight-Capability exceeded - C
  • Environmental issues-Conditions/weather/phenomena-Temp/humidity/pressure-High density altitude-Effect on equipment - C

What happened

The pilot reported that, during takeoff, the airplane became airborne with 3,000 ft of runway remaining. When the airplane was between about 25 and 40 ft above ground level (agl), its nose dropped, and the pilot then pulled back on the control stick. The pilot was able to level out the airplane and establish a 200-ft-per-minute climb rate. As the airplane approached 75 ft agl at an indicated airspeed of about 95 mph, the airplane's nose dropped to about a 30- to 45-degree nose-down attitude. The pilot again pulled back on the control stick, but he was unable to regain control of the airplane before it impacted the ground.

The pilot reported that the engine was running roughly during an initial start-up, but he stated that it ran normally during a subsequent start-up and two engine run-ups before taking off on the accident flight. A postaccident examination of the engine and airframe revealed no evidence of mechanical malfunctions or failures that would have precluded normal operation. The airplane's calculated gross weight exceeded its allowable maximum gross weight, and high-density altitude conditions existed at the time of the accident. Although these conditions likely affected the airplane's performance, the pilot was able to establish a positive climb rate after takeoff; however, he did not maintain control of the airplane as the pitch changed.

An editorial "what led to it / how to avoid it" analysis for this accident is generated separately and will appear here.

View the official NTSB docket →