Fuel Exhaustion & Starvation · NTSB WPR14FA218

NEBERT VANS RV-10 — Toledo, OR

2 fatal
DateMay 31, 2014
LocationToledo, OR
AircraftNEBERT VANS RV-10 (amateur-built)
Purpose of flightPersonal
ConditionsDay · Visual Meteorological Cond
Phase / occurrenceEnroute-climb to cruise Loss of engine power (total)
Pilot age51
Pilot total time785 hrs · Building experience
Time in type375 hrs
Fatalities2, 1 serious

Probable cause

A total loss of engine power due to fuel starvation because of a blocked fuel line that resulted from the pilot’s improper maintenance practices and the pilot’s subsequent failure to maintain adequate airspeed while attempting a forced landing, which led to the airplane exceeding its critical angle-of-attack and experiencing an aerodynamic stall.

NTSB findings

  • Aircraft-Aircraft systems-Fuel system-(general)-Incorrect service/maintenance - C
  • Personnel issues-Task performance-Maintenance-Installation-Owner/builder - C
  • Personnel issues-Task performance-Use of equip/info-Aircraft control-Pilot - C
  • Aircraft-Aircraft oper/perf/capability-Performance/control parameters-Airspeed-Not attained/maintained - C
  • Aircraft-Aircraft oper/perf/capability-Performance/control parameters-Angle of attack-Not attained/maintained - C

What happened

The pilot, who was also the builder of the experimental kit airplane, departed for a cross-country flight from his home airport. The passenger reported that, following a normal departure, the airplane continued the takeoff climb through some cloud wisps and ascended above a lower cloud cover with an overcast layer above. Suddenly, the engine experienced a total loss of power. The pilot maneuvered the airplane toward the closest airport, but, when he realized that the airplane would not be able to glide to the airport, he attempted to make an off-airport landing. The airplane stalled and then collided with terrain in an open area of a paper mill. Ground scar analysis and wreckage fragmentation revealed that the airplane descended in a steep, near-vertical, nose-down, left-wing-down attitude before it impacted terrain.

The pilot installed a fuel flow transducer about 2 to 3 weeks before the accident and used heavy applications of room temperature vulcanization (RTV) silicone to seal the fuel lines. A friend of the pilot, who was also a mechanic, reported that he had observed the pilot about a year earlier using heavy applications of RTV silicone to seal parts during a condition inspection and that he had mentioned to the pilot that this was an improper practice. A bead of RTV silicone was found in the fuel line, and it is likely that it blocked the inlet of the transducer and starved the engine of fuel. Additionally, subsequent to the loss of engine power, the pilot failed to maintain sufficient airspeed while maneuvering to locate a suitable off-airport landing site and flew the airplane beyond its critical angle-of-attack, which resulted in a stall and loss of airplane control.

An editorial "what led to it / how to avoid it" analysis for this accident is generated separately and will appear here.

View the official NTSB docket →