Loss of Control in Flight · NTSB WPR15FA016

SONEX SONEX TRIGEAR — Fawnskin, CA

1 fatal
DateOctober 20, 2014
LocationFawnskin, CA
AircraftSONEX SONEX TRIGEAR
Purpose of flightPersonal
ConditionsDay · Visual Meteorological Cond
Phase / occurrenceUncontrolled descent Collision with terr/obj (non-CFIT)
Pilot age60
Pilot total time500 hrs · Building experience
Time in typeUnknown
Fatalities1

Probable cause

The pilot's failure to maintain airspeed after takeoff, which resulted in an exceedance of the airplane's critical angle of attack and a subsequent aerodynamic stall/spin at low altitude. Contributing to the accident was the airplane's reduced climb performance due to a carbon-fouled engine cylinder, the airplane's lack of wheel pants and fairings, and the high density altitude conditions.

NTSB findings

  • Aircraft-Aircraft oper/perf/capability-Performance/control parameters-Angle of attack-Capability exceeded - C
  • Personnel issues-Action/decision-Action-Incorrect action performance-Pilot - C
  • Environmental issues-Conditions/weather/phenomena-Temp/humidity/pressure-High density altitude-Awareness of condition
  • Personnel issues-Task performance-Use of equip/info-Aircraft control-Pilot - C

What happened

The sport pilot had purchased the airplane 2 days before the accident and was returning it to his home airport. Witnesses observed the airplane shortly after takeoff over a lake near the departure airport, and noted that the airplane was below the elevation of the surrounding terrain. As the airplane approached a cove, it banked left to almost 90 degrees. The nose dropped to a nearly-vertical attitude, and the airplane descended to ground contact.

A postaccident examination of the airframe and flight controls revealed no evidence of mechanical malfunctions or failures that would have precluded normal operation. Examination of the engine determined that one of the four cylinders was carbon-fouled, which was likely the result of an overly rich fuel/air mixture due to the valve adjustment in that cylinder. Given the condition of the cylinder, the 80-horsepower (hp) engine was most likely producing only about 60 hp before the accident. The airplane was not equipped with wheel pants or fairings, which increased drag and further degraded the airplane's performance. Additionally, the density altitude at the time of the accident was over 8,200 ft.

Although the pilot had a history of sleep apnea, he was using continuous positive airway pressure (CPAP) therapy, and it is unlikely that his sleep apnea contributed to the accident. Toxicological testing detected citalopram, a prescription medication used to treat depression and panic disorder. The investigation did not determine a definitive psychiatric diagnosis, but no operational evidence of pilot impairment was identified, and it is unlikely that the pilot's use of this medication contributed to the accident.

The combination of high density altitude, airplane configuration, and cylinder fouling resulted in significantly decreased performance. It is likely that the airplane's margin above stall speed was minimal as the pilot attempted to climb the airplane after takeoff, and in his attempt to maneuver away from the rising, mountainous terrain, the pilot exceeded the airplane's critical angle of attack, which resulted in an aerodynamic stall/spin.

An editorial "what led to it / how to avoid it" analysis for this accident is generated separately and will appear here.

View the official NTSB docket →