Fuel Exhaustion & Starvation · NTSB WPR16FA035
AERO VODOCHODY L 39C — Apple Valley, CA
| Date | December 6, 2015 |
| Location | Apple Valley, CA |
| Aircraft | AERO VODOCHODY L 39C |
| Purpose of flight | Personal |
| Conditions | Day · Visual Meteorological Cond |
| Phase / occurrence | Takeoff Collision with terr/obj (non-CFIT) |
| Pilot age | 60 |
| Pilot total time | 23,223 hrs · High time |
| Time in type | 170 hrs |
| Fatalities | 2 |
Probable cause
NTSB findings
- Aircraft-Aircraft power plant-Engine (turbine/turboprop)-(general)-Failure - C
- Personnel issues-Task performance-Maintenance-(general)-Not specified - C
- Aircraft-Aircraft power plant-Engine fuel and control-Fuel controlling system-Incorrect use/operation - C
- Aircraft-Aircraft power plant-Engine fuel and control-(general)-Fatigue/wear/corrosion - C
What happened
The airline transport pilot was taking the private-pilot-rated passenger on a local flight in the former foreign-military jet trainer. After the airplane was refueled, the pilot delivered his customary 1-hour safety briefing to the passenger. The pilot subsequently taxied the airplane to the airport run-up area and, after a brief pause, to the runway. As the pilot initiated the takeoff roll, a witness observed dark gray smoke coming from the engine exhaust. When the airplane was about halfway down the runway and about 100 ft above ground level, the engine experienced a total loss of power. The airplane maintained altitude until it reached the end of the runway, at which point it rolled left, descended rapidly, and impacted the ground. A postcrash fire erupted that destroyed the majority of the airplane.
Postaccident examination of the airplane revealed no evidence of any preimpact anomalies with the airplane's control system; however, control continuity could not be confirmed due to the extensive thermal damage to the airframe. Postaccident examination of the engine revealed that thermal distress of the 2nd and 3rd stage turbine nozzles and blades led to failure of the 2nd stage turbine blades, which rendered the engine incapable of producing thrust. All the fuel nozzles were below factory allowable limits in terms of flow rate and spray pattern and failed the factory functional test procedure. The asymmetrically deteriorated conditions of the installed fuel nozzle set matched the asymmetrically deteriorated condition of the 2nd stage turbine nozzle.
The maximum metered fuel delivery pressure measured on the test bench for the fuel control unit (FCU) was 85 atmospheres (atm). The typical maximum metered fuel delivery pressure for a normally operating engine to produce maximum approved thrust is 48 to 50 atm of pressure with an absolute maximum fuel pressure of 65 atm. The FCU was adjusted back to 50 atm during the test, indicating that there was no internal fault with the FCU but rather it had been purposely adjusted to 85 atm fuel pressure.
A search of the maintenance logbooks did not reveal when or where this FCU fuel pressure adjustment occurred. During the inspection and engine performance run-up of the engine performed about 2 weeks before the accident, maintenance personnel should have noticed an overly high fuel pressure, but this did not occur, making it likely that the FCU was adjusted after the inspection. It is possible that whoever made this adjustment did not understand or appreciate the fuel nozzle condition and erroneously tried to increase the fuel pressure to compensate for the low flow rate of the fuel nozzles.
The manual adjustment of the FCU to deliver an overly high fuel pressure combined with the deteriorated condition of the fuel nozzles likely led to the heat-deteriorated condition of the 2nd and 3rd stage turbine nozzles and blades within a short period of time. Further, two of the four thermocouples that sense exhaust gas temperature had failed, which increased the likelihood of an incorrect cooler-than-actual temperature indication in the cockpit. As a result, the pilot likely did not observe any indication of engine thermal distress before the power loss.