Loss of Control in Flight · NTSB WPR16FA091

NOKES MATTHEW LANCAIR IV P — Fallbrook, CA

High-time pilot
DateApril 2, 2016
LocationFallbrook, CA
AircraftNOKES MATTHEW LANCAIR IV P (amateur-built)
Purpose of flightPersonal
ConditionsDay · Visual Meteorological Cond
Phase / occurrenceLanding Collision with terr/obj (non-CFIT)
Pilot age62
Pilot total time4,750 hrs · High time
Time in type1,200 hrs
Fatalities0, 2 serious

Probable cause

A loss of engine power during cruise for reasons that could not be determined because examination of the airplane did not reveal any anomalies that would have precluded normal operation.

NTSB findings

  • Not determined-Not determined-(general)-(general)-Unknown/Not determined - C
  • Environmental issues-Physical environment-Object/animal/substance-Ground vehicle-Effect on equipment

What happened

About 15 minutes after departing on the cross-country flight, the experimental, amateur-built airplane experienced a loss of engine power, and the private pilot considered landing on a 550-ft-long airstrip for remote-controlled aircraft. After observing numerous people on and near the runway, he subsequently decided to land on an interstate highway. Upon touching down with the landing gear retracted, the airplane slid into a car parked on the paved shoulder of the highway, fatally injuring one of the car's occupants. Video footage captured by a cell phone inside the airplane showed normal engine indications before the accident. A video taken shortly thereafter did not capture the instrument panel or engine indications; however, the engine could be heard surging.

The airplane was equipped with fuel tanks in the left and right wings, as well as a fuselage tank. The right and left wing tanks each had a capacity of 52 gallons, and the capacity of the fuselage tank was 33 gallons. The fuel system was configured so that the left wing tank connected to the fuselage tank, and the engine would draw from the fuselage tank. The fuselage tank did not have a dedicated fuel quantity gauge; the pilot stated that he knew it was full when the wing tank gauge began to indicate above zero. The pilot stated that before departing on the accident flight, the left fuel tank quantity gauge indicated 1 gallon, which corresponded to 34 gallons available.

Postaccident examination of the airframe and engine revealed no evidence of mechanical malfunctions or failures that would have precluded normal operation. A test run of the engine at low, intermediate, and high power settings was successful.

The fuselage tank was breached during the accident, and an undetermined quantity of fuel leaked out. The gascolator did not contain any fuel, and the line from the gascolator to the engine-driven fuel pump, as well as the fuel inlet line to the fuel manifold, contained no fuel. The lack of fuel in these areas, coupled with the engine surging heard on video, may be an indication of fuel starvation; however, since the investigation was unable to determine the total quantity of fuel on board the airplane, the reason for the loss of power and engine surging could not be determined.

An editorial "what led to it / how to avoid it" analysis for this accident is generated separately and will appear here.

View the official NTSB docket →