Fuel Exhaustion & Starvation · NTSB WPR17FA150
CIRRUS DESIGN CORP SR22T — SCHELLVILLE, CA
| Date | July 13, 2017 |
| Location | SCHELLVILLE, CA |
| Aircraft | CIRRUS DESIGN CORP SR22T |
| Purpose of flight | Personal |
| Conditions | Day · Visual Meteorological Cond |
| Phase / occurrence | Initial climb Aerodynamic stall/spin |
| Pilot age | 38 |
| Pilot total time | 550 hrs · Building experience |
| Time in type | Unknown |
| Fatalities | 2, 1 serious |
Probable cause
NTSB findings
- Personnel issues-Task performance-Use of equip/info-Aircraft control-Pilot - C
- Aircraft-Aircraft oper/perf/capability-Performance/control parameters-Airspeed-Not attained/maintained - C
- Aircraft-Aircraft oper/perf/capability-Performance/control parameters-Angle of attack-Not attained/maintained - C
- Personnel issues-Task performance-Use of equip/info-Use of equip/system-Pilot - C
- Aircraft-Aircraft power plant-Engine fuel and control-Fuel pump-Incorrect use/operation - C
- Personnel issues-Task performance-Use of equip/info-Use of checklist-Pilot - F
What happened
The private pilot and three passengers departed on a personal cross-county flight. Several witnesses located at or near the airport reported that, while the airplane was climbing, they heard the engine "sputter" or "pop" a few times as the airplane flew over their position. Subsequently, they heard a louder sound and, shortly afterward, observed the deployment of the airplane's parachute system. Most of the witnesses observed the airplane descending just before they lost sight of it at tree-top level, which was just before the airplane impacted the ground. A review of the airplane's flight data revealed that, shortly after takeoff, the airplane's engine lost power. At that time, the airplane's airspeed decreased and approached the stall speed; the stall warning system activated twice. From the first stall warning to the end of the data, the airplane's airspeed was between 71 and 75 knots and the airplane was in a bank of about 27°; the airplane's stall speed is 76 knots at a bank angle of 30°. The airplane's parachute system was deployed when the airplane's altitude was about 130 ft mean sea level.
When engine power was lost, the pilot failed to maintain an adequate airspeed and did not follow the emergency procedures for a low-altitude engine failure in the Cirrus SR22T Pilot's Operating Handbook (POH), which were to lower the nose, establish an appropriate glide airspeed, and accomplish a landing straight ahead, turning only to avoid obstructions.
Postaccident examination of the airframe and engine revealed no anomalies that would have precluded normal operation. However, examination of the top spark plugs in the ignition system revealed that their insulators were dark in color, consistent with a rich fuel/air mixture.
The POH stated that the electric fuel pump switch must be set to the "Boost" position for takeoff and climbout. However, the flight data indicated an excessively high fuel flow to the engine that was consistent with the electric fuel pump switch selected to the "High Boost/Prime" position (which is used for priming the fuel pump before engine start) at the time of the loss of engine power. The flight data indicated that the fuel flow increased and peaked at a level that was about 6.5% higher than the average climbout fuel flow just before the power loss. The National Transportation Safety Board's investigation of an accident involving another Cirrus SR22T airplane found that the airplane experienced an engine power loss following that pilot's inadvertent activation of the High Boost/Prime switch, and flight data from that airplane revealed a similar increase in the fuel flow before the loss of engine power.
For this accident, both the fuel flow and manifold pressure exceeded the manufacturer's parameters in the POH, peaking about the time of the engine power loss. Further, given that the engine's speed exceeded the manufacturer's upper warning range just before the loss of engine power, the engine components and the fuel system were likely operating effectively before the loss of power. Thus, it is likely that the accident pilot improperly selected the High Boost/Prime position during the climbout, which resulted in the excessive fuel flow to the engine and the subsequent loss of engine power.