Stall / Spin · NTSB WPR17FA171

CESSNA 172N — Big Bear, CA

2 fatal
DateJuly 29, 2017
LocationBig Bear, CA
AircraftCESSNA 172N
Purpose of flightPersonal
ConditionsDay · Visual Meteorological Cond
Phase / occurrenceInitial climb Aerodynamic stall/spin
Pilot age30
Pilot total time750 hrs · Building experience
Time in type225 hrs
Fatalities2

Probable cause

The pilot's exceedance of the airplane's critical angle of attack during takeoff in high density altitude conditions, which resulted in an aerodynamic stall, loss of control, and subsequent impact with terrain.

NTSB findings

  • Personnel issues-Task performance-Use of equip/info-Aircraft control-Pilot - C
  • Environmental issues-Conditions/weather/phenomena-Temp/humidity/pressure-High density altitude-Effect on operation - C
  • Aircraft-Aircraft oper/perf/capability-Performance/control parameters-Angle of attack-Not attained/maintained - C
  • Personnel issues-Task performance-Use of equip/info-Use of equip/system-Pilot
  • Aircraft-Aircraft oper/perf/capability-Performance/control parameters-Airspeed-Not attained/maintained - C
  • Aircraft-Aircraft oper/perf/capability-Performance/control parameters-Climb rate-Not attained/maintained
  • Aircraft-Aircraft power plant-Engine controls-Mixture control-Incorrect use/operation

What happened

The commercial pilot and passenger departed in the airplane from the airport, which was located at an elevation of 6,752 ft mean sea level (msl). Airport surveillance video showed that the airplane became increasingly slow during the initial climb after takeoff. A witness reported that, as the airplane approached the end of the runway, it stopped climbing and entered a nose-high pitch attitude that the witness described as "hanging by the prop." The airplane then turned 90° to the downwind leg of the airport traffic pattern and sank as the wings rocked back and forth before it disappeared behind trees. The wreckage orientation indicated that the airplane maintained a southerly heading before it descended into the tree line. The airplane impacted the ground in a nose-down attitude with partial forward bending of the tail, consistent with an aerodynamic stall. Postaccident examination of the airplane did not reveal any preimpact anomalies.

The density altitude about the time of the accident exceeded 9,100 ft msl. The effects of high density altitude conditions on takeoff performance include increased takeoff roll distance and reduced rate of climb. Review of performance charts indicated that the airplane should have been able to climb at a rate around 440 ft per minute; however, the video indicated that the airplane was climbing at a rate of 340 ft per minute. It is likely that, experiencing degraded airplane performance due to the density altitude, the pilot responded by increasing the airplane's pitch attitude in an attempt to improve its rate of climb. The pilot subsequently exceeded the airplane's critical angle of attack, which resulted in an aerodynamic stall and impact with terrain.

The pilot's primary flight experience was in turbine engine-equipped rotorcraft, and he had recently received a checkout in the accident airplane make and model that included high density altitude operation and mixture leaning procedures. The airplane's mixture control was found in the full rich position after the accident; however, the position of the control before and during the takeoff could not be determined. If the pilot departed in the high density altitude environment without leaning the fuel/air mixture control or subsequently enrichened the fuel/air mixture control to troubleshoot the airplane's reduced takeoff performance, this would have further reduced the available engine power and the airplane's climb rate.

An editorial "what led to it / how to avoid it" analysis for this accident is generated separately and will appear here.

View the official NTSB docket →