Mechanical & Engine Failure · NTSB WPR19FA093

Piper PA23 — Pahokee, FL

5 fatal High-time pilot
DateMarch 8, 2019
LocationPahokee, FL
AircraftPiper PA23
Purpose of flightUnknown
ConditionsDay · Visual Meteorological Cond
Phase / occurrenceEnroute-cruise Loss of engine power (partial)
Pilot age45
Pilot total time2,100 hrs · Experienced
Time in typeUnknown
Fatalities5

Probable cause

The pilot's failure to maintain control of the airplane while maneuvering for landing with one engine inoperative following a loss of engine power for reasons that could not be determined based on the available information.

NTSB findings

  • Personnel issues-Task performance-Use of equip/info-Aircraft control-Pilot - C
  • Aircraft-Aircraft oper/perf/capability-Performance/control parameters-(general)-Not attained/maintained
  • Not determined-Not determined-(general)-(general)-Unknown/Not determined
  • Aircraft-Aircraft power plant-Power plant-(general)-Inoperative

What happened

While descending from cruise altitude toward the destination airport, the pilot reported to air traffic control that he needed to divert to a closer airport because the left engine was "misfiring" and that he was going to "shut it down." Radar data indicated that the airplane flew toward the diversion airport and continued to maneuver south past the airport, where radar contact was lost around 700 ft mean sea level. The airplane subsequently impacted a lake about 1/2 mile west of the airport.

Data from the airplane's engine monitoring system revealed a drop in left engine exhaust gas temperature (EGT), cylinder head temperature (CHT), and fuel flow values near the end of the flight. These values then increased again for a few minutes before decreasing a second time. The left engine fuel flow value for the last 3 minutes of the data was 0, and the left propeller was found in the feathered position, consistent with the pilot having shut down and secured the engine in flight.

Review of the airframe maintenance logbook indicated that several airframe-related fuel system components were replaced during the 4 months before the accident. An entry in the left engine logbook about 4 days before the accident stated that the left engine No. 5 CHT was fluctuating and that a loss of 300 rpm was experienced when testing the right magneto in flight; however, this issue could not be duplicated on the ground, and the airplane was returned to service. Fuel residue was observed on and around the left engine's electric fuel pump. The pump was removed and functionally tested, during which two leaks were found during pressure tests; however, the effect of these leaks on engine operation could not be determined. No other anomalies of the airframe fuel system were observed; however, the system was heavily fragmented and had been submerged in water for several days before recovery.

Based on the available information, the reason for the reported loss of engine power and the extent to which the left engine may have been able to continue to produce power could not be determined. Additionally, the reason for the pilot's low-altitude maneuvering in the vicinity of the runway could not be determined; however, it is likely that the pilot failed to maintain airspeed while maneuvering for landing with the left engine inoperative, which resulted in a loss of control and impact with water.

An editorial "what led to it / how to avoid it" analysis for this accident is generated separately and will appear here.

View the official NTSB docket →