Fuel Exhaustion & Starvation · NTSB WPR19FA251

Piper PA18 — Hood River, OR

2 fatal High-time pilot
DateSeptember 6, 2019
LocationHood River, OR
AircraftPiper PA18
Purpose of flightPersonal
ConditionsDay · Visual Meteorological Cond
Phase / occurrenceTakeoff Loss of control in flight
Pilot age55
Pilot total time21,012 hrs · High time
Time in type0 hrs
Fatalities2

Probable cause

The total loss of engine power shortly after takeoff as a result of the private pilot’s failure to ensure the fuel selector was in the appropriate position and the certified flight instructor’s exceedance of the airplane’s critical angle of attack at the time of the engine power loss, which resulted in an aerodynamic stall and loss of airplane control.

NTSB findings

  • Personnel issues-Task performance-Use of equip/info-Use of equip/system-Pilot
  • Aircraft-Aircraft systems-Fuel system-Fuel selector/shutoff valve-Unintentional use/operation
  • Personnel issues-Task performance-Use of equip/info-Aircraft control-Instructor/check pilot
  • Aircraft-Aircraft oper/perf/capability-Performance/control parameters-Angle of attack-Capability exceeded

What happened

Witnesses observed the airplane takeoff, and one witness noted its nose-high attitude during takeoff. They then heard the engine lose power. The airplane subsequently pitched down and began a rotation to the right before impacting the ground just north of the runway.

First responders reported that the fuel selector valve was found in the OFF position when they arrived at the accident site, and they also noted fuel leaking from the airplane. Further examination of the airplane revealed the fuel selector indicator plate displayed a red witness mark adjacent to the fuel selector pointer under one of the OFF-indicator marks, which is an indication the selector was in the OFF position at the time of impact. No evidence of mechanical malfunctions or failures were identified that would have precluded normal operation. Because the engine lost power during takeoff, it is possible that there was enough residual fuel in the fuel lines to start the engine and taxi to the runway, even with the selector in the OFF position.

The private pilot was seated in the front seat and the certified flight instructor was seated in the rear seat. The fuel selector was located on the left cabin wall closest to the private pilot; it is likely the private pilot failed to check the position before takeoff.

When the airplane departed, it was about 21 pounds over the maximum takeoff weight. An increase in the airplane’s weight would have an adverse effect on stability and controllability. Because the airplane was already in a nose-high attitude when the engine lost power, the airplane likely stalled. The increased weight and low altitude when the power loss occurred prevented the pilots from recovering.

Postmortem toxicology testing detected quinine in the certified flight instructor’s blood and urine at a level that was not quantified; therefore, the amount detected was likely from a tonic drink containing quinine rather than ingestion of the drug and would not have been impairing.

An editorial "what led to it / how to avoid it" analysis for this accident is generated separately and will appear here.

View the official NTSB docket →