Loss of Control in Flight · NTSB WPR22FA216
CESSNA 336 — Porterville, CA
| Date | June 18, 2022 |
| Location | Porterville, CA |
| Aircraft | CESSNA 336 |
| Purpose of flight | Personal |
| Conditions | Day · Visual Meteorological Cond |
| Phase / occurrence | Enroute-cruise Collision with terr/obj (non-CFIT) |
| Pilot age | 31 |
| Pilot total time | 690 hrs · Building experience |
| Time in type | 35 hrs |
| Fatalities | 1 |
Probable cause
NTSB findings
- Aircraft-Aircraft systems-Flight control system-Elevator control system-Not specified
- Aircraft-Aircraft systems-Flight control system-Elevator control system-Incorrect service/maintenance
- Aircraft-Aircraft systems-Flight control system-Elevator control system-Inadequate inspection
- Personnel issues-Task performance-Maintenance-Installation-Maintenance personnel
What happened
Shortly after takeoff, the pilot transmitted over the radio that he had lost “almost all pitch control,” but thought that he would be able to return and land at the departure airport. Automatic Dependent Surveillance Broadcast (ADS-B) data showed that the airplane climbed to about 1,550 ft mean sea level (msl) before entering a descending right 180° turn toward the departure airport. The airplane leveled off about 1,000 ft msl and continued toward the airport. About two minutes later, the airplane entered a descent from 975 ft that continued to ground contact.
Witnesses reported that they observed the airplane flying at low altitude when it suddenly descended into the ground in a steep, nose-low, wings-level attitude.
Postaccident examination of the wreckage revealed that the bolt, castellated nut, and cotter pin that connected the balance weight to the elevator control assembly were missing. Soot was observed within the area of both connection points, including where the bolt and washer would have been installed, consistent with the hardware not being installed at the time of the accident. It is likely that the bolt separated while in flight, resulting in a loss of elevator pitch control. The missing bolt, nut, washer, and cotter pin were not located.
The airplane was painted and returned to service about 28 days before the accident, which included removal and reinstallation of all the flight controls. It could not be determined if the securing hardware (nut and cotter pin) were installed at the time of the reinstallation of the elevator.
Toxicology testing of the pilot revealed the presence of ethanol in liver tissue; however, the detected ethanol likely was from postmortem production. Thus, it is unlikely that ethanol contributed to the accident.